HL incident on 2015-10-05 — TX

Operator
Enterprise Products Operating Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,130,319
Incident datetime
2015-10-05 09:45
Report number
Location
TX
Narrative
Tank was out-of-service for a scheduled API-653 inspection. Upon reintroducing product after repairs, a small pool of gasoline was observed by operations personnel on the ground beside the base of the tank. All product was removed from the tank and the tank was blocked in. The tank was made safe for entry and the spilled product remediated. Upon entry, a 1/4-inch hole was discovered in the tank floor. The hole was drilled prior to making floor repairs to check for hazardous vapors under the tank floor. The area of the tank floor where the hole was located was cut out and a new steel patch plate was installed. In addition, a thorough floor inspection was completed before returning the tank to service. All remediation and repairs are complete and the tank was returned to service.
Detailed record list
Report Received Date
2015-10-30 00:00:00
Iyear
2015
Report Number
20150387
Supplemental Number
21116
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-10-05 11:18:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.2
Recovered Bbls
0.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-10-05 09:45:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Was Shut-In, Terminal And Pipelines Continued Operating
On Site Datetime
2015-10-05 09:45:00
Nrc Rpt Datetime
2015-10-05 12:02:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
North Port Arthur Terminal
Segment Name
Refined Products Tankage
Onshore State Abbreviation
Tx
Onshore Postal Code
77640
Onshore City Name
Port Arthur
Onshore County Name
Jefferson
Designated Location
Milepost/valve Station
Designated Name
Tk 5200
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Single Bottom System
Tank Type
Atmospheric
Installation Year
2015
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
0.5
Puncture Circum
0.3
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
22
Est Cost Prop Damage
1130319
Est Cost Emergency
0
Est Cost Environmental
43000
Est Cost Other
0
Prpty
1173341
Accident Psig
0
Mop Psig
0
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Release discovered during operator rounds. No controller actions impacted release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related No Proc Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
M*** P*****
Preparer Title
Sr. Compliance Specialist
Preparer Email
M*******@e****.com
Preparer Telephone
713-381-5897
Prepared Date
2016-02-11 00:00:00
Authorizer Name
M*** P*****
Authorizer Telephone
713-381-5897
Authorizer Title
Sr. Compliance Specialist
Authorizer Email
M*******@e****.com
Narrative
Tank was out-of-service for a scheduled API-653 inspection. Upon reintroducing product after repairs, a small pool of gasoline was observed by operations personnel on the ground beside the base of the tank. All product was removed from the tank and the tank was blocked in. The tank was made safe for entry and the spilled product remediated. Upon entry, a 1/4-inch hole was discovered in the tank floor. The hole was drilled prior to making floor repairs to check for hazardous vapors under the tank floor. The area of the tank floor where the hole was located was cut out and a new steel patch plate was installed. In addition, a thorough floor inspection was completed before returning the tank to service. All remediation and repairs are complete and the tank was returned to service.
Report Received Date 2015-10-30 00:00:00
Iyear 2015
Report Number 20150387
Supplemental Number 21116
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-10-05 11:18:00
Location Latitude 29.91125 Google Maps OpenStreetMap
Location Longitude -94.010521 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.2
Recovered Bbls 0.2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-10-05 09:45:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank Was Shut-In, Terminal And Pipelines Continued Operating
On Site Datetime 2015-10-05 09:45:00
Nrc Rpt Datetime 2015-10-05 12:02:00
Nrc Rpt Num 1130130 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name North Port Arthur Terminal
Segment Name Refined Products Tankage
Onshore State Abbreviation Tx
Onshore Postal Code 77640
Onshore City Name Port Arthur
Onshore County Name Jefferson
Designated Location Milepost/valve Station
Designated Name Tk 5200
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Intrastate
Item Involved Tank/vessel
Tank Vessel Subtype Single Bottom System
Tank Type Atmospheric
Installation Year 2015
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 0.5
Puncture Circum 0.3
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 22
Est Cost Prop Damage 1130319
Est Cost Emergency 0
Est Cost Environmental 43000
Est Cost Other 0
Prpty 1173341
Accident Psig 0
Mop Psig 0
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Release discovered during operator rounds. No controller actions impacted release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related No Proc Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name M*** P*****
Preparer Title Sr. Compliance Specialist
Preparer Email M*******@e****.com
Preparer Telephone 713-381-5897
Prepared Date 2016-02-11 00:00:00
Authorizer Name M*** P*****
Authorizer Telephone 713-381-5897
Authorizer Title Sr. Compliance Specialist
Authorizer Email M*******@e****.com
Narrative Tank was out-of-service for a scheduled API-653 inspection. Upon reintroducing product after repairs, a small pool of gasoline was observed by operations personnel on the ground beside the base of the tank. All product was removed from the tank and the tank was blocked in. The tank was made safe for entry and the spilled product remediated. Upon entry, a 1/4-inch hole was discovered in the tank floor. The hole was drilled prior to making floor repairs to check for hazardous vapors under the tank floor. The area of the tank floor where the hole was located was cut out and a new steel patch plate was installed. In addition, a thorough floor inspection was completed before returning the tank to service. All remediation and repairs are complete and the tank was returned to service.

All rights reserved. Copyright © by ClearPHMSA