HL incident on 2015-09-25 — GA

Operator
Colonial Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2015-09-25 23:31
Report number
Location
GA
Narrative
On 9/25/2015, at 23:00, the gasket at the four-inch vent pipe flange failed on the line 02 prover at houston station. The release was discovered by an employee at 23:31 and the line was immediately shutdown and the station and prover isolated. A technician responded at approximately 00:15 on 9/26/2015 and completed further isolation (lockout/tagout) and draining of the prover. The line was restarted on 9/26/15 at 01:38. On 9/26/15 at 09:20 the texas state emergency response center was notified and they in turn notified tceq. The nrc was notified on monday 9/28/2015 at 15:11 when it was determined that the cost of cleanup and recovery were likely going to exceed $50,000. The failed gasket was installed by a qualified colonial technician in january 2015 following a water draw of the prover. Incident analysis of the event determined that the basic causes of the gasket failure were: 1.) failure to follow colonial's cm-111 bolted connections procedure when the gasket was replaced in january 2015. 2.) failure to follow colonial's material & equipment specification ms-07-06 for proper marking of gaskets with date of manufacture and receipt when the gasket was received at the warehouse. Following the determination that the technician's actions were a contributing factor to the accident, the technician's oq qualification to perform flange bolting procedures was disqualified in accordance with colonial's operator qualification program manual. As a remedial action, the technician was required to re-qualify using the performance verification method. Two corrective actions have been identified to improve the process of tracking gasket shelf life.
Detailed record list
Report Received Date
2015-10-22 00:00:00
Iyear
2015
Report Number
20150369
Supplemental Number
20997
Report Type
Supplemental Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1000 Lake St.
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009
Local Datetime
2015-09-25 23:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
38.7
Recovered Bbls
38.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-09-25 23:31:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-09-25 23:31:00
Restart Datetime
2015-09-26 01:38:00
On Site Datetime
2015-09-25 23:31:00
Nrc Rpt Datetime
2015-09-28 15:04:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Houston Station
Segment Name
Line 2 Prover
Onshore State Abbreviation
Tx
Onshore Postal Code
77506
Onshore City Name
Pasadena
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Location 0120
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Meter/prover
Installation Year
2010
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
5500
Est Cost Prop Damage
500
Est Cost Emergency
45000
Est Cost Environmental
249000
Est Cost Other
0
Prpty
300000
Accident Psig
156
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release resulted from a failed gasket.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Installation Ind
Yes
Preparer Name
K**** M****
Preparer Title
Compliance Coordinator
Preparer Email
K*****@c******.com
Preparer Telephone
601-765-9168
Preparer Fax
770-754-8489
Prepared Date
2015-12-17 00:00:00
Authorizer Name
D*** L*****
Authorizer Telephone
678-7622872
Authorizer Title
Manager Phmsa Regulatory Compliance
Authorizer Email
D*******@c******.com
Narrative
On 9/25/2015, at 23:00, the gasket at the four-inch vent pipe flange failed on the line 02 prover at houston station. The release was discovered by an employee at 23:31 and the line was immediately shutdown and the station and prover isolated. A technician responded at approximately 00:15 on 9/26/2015 and completed further isolation (lockout/tagout) and draining of the prover. The line was restarted on 9/26/15 at 01:38. On 9/26/15 at 09:20 the texas state emergency response center was notified and they in turn notified tceq. The nrc was notified on monday 9/28/2015 at 15:11 when it was determined that the cost of cleanup and recovery were likely going to exceed $50,000. The failed gasket was installed by a qualified colonial technician in january 2015 following a water draw of the prover. Incident analysis of the event determined that the basic causes of the gasket failure were: 1.) failure to follow colonial's cm-111 bolted connections procedure when the gasket was replaced in january 2015. 2.) failure to follow colonial's material & equipment specification ms-07-06 for proper marking of gaskets with date of manufacture and receipt when the gasket was received at the warehouse. Following the determination that the technician's actions were a contributing factor to the accident, the technician's oq qualification to perform flange bolting procedures was disqualified in accordance with colonial's operator qualification program manual. As a remedial action, the technician was required to re-qualify using the performance verification method. Two corrective actions have been identified to improve the process of tracking gasket shelf life.
Report Received Date 2015-10-22 00:00:00
Iyear 2015
Report Number 20150369
Supplemental Number 20997
Report Type Supplemental Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1000 Lake St.
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009
Local Datetime 2015-09-25 23:30:00
Location Latitude 29.71897 Google Maps OpenStreetMap
Location Longitude -95.1793 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 38.7
Recovered Bbls 38.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-09-25 23:31:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-09-25 23:31:00
Restart Datetime 2015-09-26 01:38:00
On Site Datetime 2015-09-25 23:31:00
Nrc Rpt Datetime 2015-09-28 15:04:00
Nrc Rpt Num 1129595 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Houston Station
Segment Name Line 2 Prover
Onshore State Abbreviation Tx
Onshore Postal Code 77506
Onshore City Name Pasadena
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Location 0120
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Meter/prover
Installation Year 2010
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 5500
Est Cost Prop Damage 500
Est Cost Emergency 45000
Est Cost Environmental 249000
Est Cost Other 0
Prpty 300000
Accident Psig 156
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release resulted from a failed gasket.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Installation Ind Yes
Preparer Name K**** M****
Preparer Title Compliance Coordinator
Preparer Email K*****@c******.com
Preparer Telephone 601-765-9168
Preparer Fax 770-754-8489
Prepared Date 2015-12-17 00:00:00
Authorizer Name D*** L*****
Authorizer Telephone 678-7622872
Authorizer Title Manager Phmsa Regulatory Compliance
Authorizer Email D*******@c******.com
Narrative On 9/25/2015, at 23:00, the gasket at the four-inch vent pipe flange failed on the line 02 prover at houston station. The release was discovered by an employee at 23:31 and the line was immediately shutdown and the station and prover isolated. A technician responded at approximately 00:15 on 9/26/2015 and completed further isolation (lockout/tagout) and draining of the prover. The line was restarted on 9/26/15 at 01:38. On 9/26/15 at 09:20 the texas state emergency response center was notified and they in turn notified tceq. The nrc was notified on monday 9/28/2015 at 15:11 when it was determined that the cost of cleanup and recovery were likely going to exceed $50,000. The failed gasket was installed by a qualified colonial technician in january 2015 following a water draw of the prover. Incident analysis of the event determined that the basic causes of the gasket failure were: 1.) failure to follow colonial's cm-111 bolted connections procedure when the gasket was replaced in january 2015. 2.) failure to follow colonial's material & equipment specification ms-07-06 for proper marking of gaskets with date of manufacture and receipt when the gasket was received at the warehouse. Following the determination that the technician's actions were a contributing factor to the accident, the technician's oq qualification to perform flange bolting procedures was disqualified in accordance with colonial's operator qualification program manual. As a remedial action, the technician was required to re-qualify using the performance verification method. Two corrective actions have been identified to improve the process of tracking gasket shelf life.

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