HL incident on 2015-09-19 — OK

Operator
Magellan Terminals Holdings, Lp
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$3,000
Incident datetime
2015-09-19 19:45
Report number
Location
OK
Narrative
Operations identified product at the surface over lateral line to tank 311. Investigation discovered a pinhole leak on a dead-leg section of pipe attached to the line. The dead-leg section of pipe was cutout prior to returning the tank lateral line back to service. Impacted soil was removed and replaced with fresh soil. Telephonic notice to the national response center was made based on total costs exceeding $50,000.
Detailed record list
Report Received Date
2015-10-15 00:00:00
Iyear
2015
Report Number
20150365
Supplemental Number
20823
Report Type
Original Final
Operator Id
Name
Magellan Terminals Holdings, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2015-09-19 19:45:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
13.21
Recovered Bbls
13.21
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-09-19 19:45:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Affected Mline Was Idle At The Time Of The Discovery
On Site Datetime
2015-09-19 19:45:00
Nrc Rpt Datetime
2015-09-19 21:15:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Galena Park Terminal
Segment Name
Terminal No. 474
Onshore State Abbreviation
Tx
Onshore Postal Code
77547
Onshore City Name
Galena Park
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
42
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
30
Pipe Wall Thickness
0.375
Pipe Smys
24000
Pipe Specification
Unknown
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1985
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
500
Est Cost Prop Damage
3000
Est Cost Emergency
9500
Est Cost Environmental
0
Est Cost Other
40000
Est Cost Other Details
Soil Excavation, Disposal & Replacement
Prpty
53000
Accident Psig
70
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Field Exam Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
7:00 O'clock Position Internal Metal Loss
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7377
Prepared Date
2015-10-15 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
Operations identified product at the surface over lateral line to tank 311. Investigation discovered a pinhole leak on a dead-leg section of pipe attached to the line. The dead-leg section of pipe was cutout prior to returning the tank lateral line back to service. Impacted soil was removed and replaced with fresh soil. Telephonic notice to the national response center was made based on total costs exceeding $50,000.
Report Received Date 2015-10-15 00:00:00
Iyear 2015
Report Number 20150365
Supplemental Number 20823
Report Type Original Final
Operator Id 31580 PHMSA Enforcement
Name Magellan Terminals Holdings, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2015-09-19 19:45:00
Location Latitude 29.74863 Google Maps OpenStreetMap
Location Longitude -95.20251 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 13.21
Recovered Bbls 13.21
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-09-19 19:45:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Affected Mline Was Idle At The Time Of The Discovery
On Site Datetime 2015-09-19 19:45:00
Nrc Rpt Datetime 2015-09-19 21:15:00
Nrc Rpt Num 1128918 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Galena Park Terminal
Segment Name Terminal No. 474
Onshore State Abbreviation Tx
Onshore Postal Code 77547
Onshore City Name Galena Park
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 42
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 30
Pipe Wall Thickness 0.375
Pipe Smys 24000
Pipe Specification Unknown
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1985
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 500
Est Cost Prop Damage 3000
Est Cost Emergency 9500
Est Cost Environmental 0
Est Cost Other 40000
Est Cost Other Details Soil Excavation, Disposal & Replacement
Prpty 53000
Accident Psig 70
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Water Acid Ind Yes
Int Field Exam Basis Ind Yes
Int Other Loc Ind Yes
Corrosion Location Details 7:00 O'clock Position Internal Metal Loss
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name K****** L* L*******
Preparer Title Sr. Compliance Coordinator
Preparer Email K***********@m*********.com
Preparer Telephone 918-574-7315
Preparer Fax 918-574-7377
Prepared Date 2015-10-15 00:00:00
Authorizer Name K****** L* L*******
Authorizer Telephone 918-574-7315
Authorizer Title Sr. Compliance Coordinator
Authorizer Email K***********@m*********.com
Narrative Operations identified product at the surface over lateral line to tank 311. Investigation discovered a pinhole leak on a dead-leg section of pipe attached to the line. The dead-leg section of pipe was cutout prior to returning the tank lateral line back to service. Impacted soil was removed and replaced with fresh soil. Telephonic notice to the national response center was made based on total costs exceeding $50,000.

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