HL incident on 2015-09-16 — OH

Operator
Tesoro Logistics Operations Llc - Southern California
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$6,000
Incident datetime
2015-09-16 06:35
Report number
Location
OH
Narrative
On september 16, 2015 a contractor working at the tesoro long beach terminal (lbt) noted vacuum gas oil (vgo) in the secondary containment of the aboveground piping vault. Pipelines running through the vault were idle when the loss of containment was discovered. There were no injuries or impact to the community. It was calculated from average gauges of the oil and water interface within the vault that approximately 70 bbl of vgo leaked from an isolating flange on mov-824 on the t-14 pipeline and was fully contained within secondary containment. It was immediately cleaned up, and the pipeline returned to service at 09:35 on september 18, 2015. A pressure of at least 200 psi was experienced by the t-14 line on september 15, 2015. However, the exact pressure cannot be determined. The monitoring system at lbt was only configured to register pressures up to 200 psi on the t-14 line.
Detailed record list
Report Received Date
2015-10-14 00:00:00
Iyear
2015
Report Number
20150363
Supplemental Number
21317
Report Type
Supplemental Final
Operator Id
Name
Tesoro Logistics Operations Llc - Southern California
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2015-09-15 12:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Other
Commodity Details
Vacuum Gas Oil
Unintentional Release Bbls
70
Recovered Bbls
70
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2015-09-16 06:35:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Line Was Already Shut Down At The Time Of Discovery.
On Site Datetime
2015-09-16 07:00:00
Nrc Rpt Datetime
2015-09-16 07:28:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Automatic
Num Pub Evacuated
0
Pipe Fac Name
Long Beach Terminal
Segment Name
T-14
Onshore State Abbreviation
Ca
Onshore Postal Code
90813
Onshore City Name
Long Beach
Onshore County Name
Los Angeles County
Designated Location
Milepost/valve Station
Designated Name
Vault 312
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Flange Assembly
Installation Year
2015
Material Involved
Material Other Than Carbon Steel
Material Details
G10 Gasket With Steel Washers
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
3500
Est Cost Prop Damage
6000
Est Cost Emergency
6000
Est Cost Environmental
0
Est Cost Other
0
Prpty
15500
Accident Psig
200
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
2600
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
No
Cpm Functional Ind
No
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Overpressure Ind
Yes
Preparer Name
H**** M****
Preparer Title
Senior Regulatory Compliance Specialist
Preparer Email
H************@t******.com
Preparer Telephone
210-626-4901
Prepared Date
2016-04-18 00:00:00
Authorizer Name
A**** W* M*******
Authorizer Telephone
210-626-6343
Authorizer Title
Director Compliance-Logistics
Authorizer Email
A***************@t******.com
Narrative
On september 16, 2015 a contractor working at the tesoro long beach terminal (lbt) noted vacuum gas oil (vgo) in the secondary containment of the aboveground piping vault. Pipelines running through the vault were idle when the loss of containment was discovered. There were no injuries or impact to the community. It was calculated from average gauges of the oil and water interface within the vault that approximately 70 bbl of vgo leaked from an isolating flange on mov-824 on the t-14 pipeline and was fully contained within secondary containment. It was immediately cleaned up, and the pipeline returned to service at 09:35 on september 18, 2015. A pressure of at least 200 psi was experienced by the t-14 line on september 15, 2015. However, the exact pressure cannot be determined. The monitoring system at lbt was only configured to register pressures up to 200 psi on the t-14 line.
Report Received Date 2015-10-14 00:00:00
Iyear 2015
Report Number 20150363
Supplemental Number 21317
Report Type Supplemental Final
Operator Id 38933 PHMSA Enforcement
Name Tesoro Logistics Operations Llc - Southern California
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2015-09-15 12:30:00
Location Latitude 33.771038 Google Maps OpenStreetMap
Location Longitude -118.225012 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Other
Commodity Details Vacuum Gas Oil
Unintentional Release Bbls 70
Recovered Bbls 70
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2015-09-16 06:35:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Line Was Already Shut Down At The Time Of Discovery.
On Site Datetime 2015-09-16 07:00:00
Nrc Rpt Datetime 2015-09-16 07:28:00
Nrc Rpt Num 1128627 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Automatic
Num Pub Evacuated 0
Pipe Fac Name Long Beach Terminal
Segment Name T-14
Onshore State Abbreviation Ca
Onshore Postal Code 90813
Onshore City Name Long Beach
Onshore County Name Los Angeles County
Designated Location Milepost/valve Station
Designated Name Vault 312
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Flange Assembly
Installation Year 2015
Material Involved Material Other Than Carbon Steel
Material Details G10 Gasket With Steel Washers
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 3500
Est Cost Prop Damage 6000
Est Cost Emergency 6000
Est Cost Environmental 0
Est Cost Other 0
Prpty 15500
Accident Psig 200
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 2600
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind No
Cpm Functional Ind No
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Overpressure Ind Yes
Preparer Name H**** M****
Preparer Title Senior Regulatory Compliance Specialist
Preparer Email H************@t******.com
Preparer Telephone 210-626-4901
Prepared Date 2016-04-18 00:00:00
Authorizer Name A**** W* M*******
Authorizer Telephone 210-626-6343
Authorizer Title Director Compliance-Logistics
Authorizer Email A***************@t******.com
Narrative On september 16, 2015 a contractor working at the tesoro long beach terminal (lbt) noted vacuum gas oil (vgo) in the secondary containment of the aboveground piping vault. Pipelines running through the vault were idle when the loss of containment was discovered. There were no injuries or impact to the community. It was calculated from average gauges of the oil and water interface within the vault that approximately 70 bbl of vgo leaked from an isolating flange on mov-824 on the t-14 pipeline and was fully contained within secondary containment. It was immediately cleaned up, and the pipeline returned to service at 09:35 on september 18, 2015. A pressure of at least 200 psi was experienced by the t-14 line on september 15, 2015. However, the exact pressure cannot be determined. The monitoring system at lbt was only configured to register pressures up to 200 psi on the t-14 line.

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