HL incident on 2015-09-11 — TX

Operator
Plains Pipeline, L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$6,900
Incident datetime
2015-09-11 09:15
Report number
Location
TX
Narrative
Approximately 2 bbls of crude oil were released as a result of two failed insulator gaskets. The cause of the release was determined to be improper installation during construction. Both gaskets were replaced with a different type of gasket and verified for proper working condition. In addition, plains operators verified all gaskets were properly torqued. Furthermore, plains created a notification and awareness report (nar), to be sent to all relevant employees in order to help prevent reoccurrence.
Detailed record list
Report Received Date
2015-10-09 00:00:00
Iyear
2015
Report Number
20150359
Supplemental Number
20813
Report Type
Original Final
Operator Id
Name
Plains Pipeline, L.p.
Operator Street Address
333 Clay Street, Suite 1900
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-09-11 09:15:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-09-11 09:15:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-09-11 09:15:00
Restart Datetime
2015-09-14 13:00:00
On Site Datetime
2015-09-11 09:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Midland (Iraan) Terminal
Segment Name
Sunrise To Midland 16"
Onshore State Abbreviation
Tx
Onshore Postal Code
79706
Onshore City Name
Midland
Onshore County Name
Midland
Designated Location
Milepost/valve Station
Designated Name
1.22
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Other
Item Involved Details
Insulating Gasket
Installation Year
2015
Material Involved
Material Other Than Carbon Steel
Material Details
Phenolic Material
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
6900
Est Cost Emergency
1600
Est Cost Environmental
0
Est Cost Other
0
Prpty
8600
Accident Psig
637
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Installation Ind
Yes
Preparer Name
C******* C*****
Preparer Title
Compliance Specialist
Preparer Email
C*******@p****.com
Preparer Telephone
713-993-5080
Preparer Fax
713-646-4310
Prepared Date
2015-10-09 00:00:00
Authorizer Name
T***** M*****
Authorizer Telephone
713-646-4109
Authorizer Title
Sr Dir Of Environmental And Regulatory Compliance
Authorizer Email
T*******@p****.com
Narrative
Approximately 2 bbls of crude oil were released as a result of two failed insulator gaskets. The cause of the release was determined to be improper installation during construction. Both gaskets were replaced with a different type of gasket and verified for proper working condition. In addition, plains operators verified all gaskets were properly torqued. Furthermore, plains created a notification and awareness report (nar), to be sent to all relevant employees in order to help prevent reoccurrence.
Report Received Date 2015-10-09 00:00:00
Iyear 2015
Report Number 20150359
Supplemental Number 20813
Report Type Original Final
Operator Id 300 PHMSA Enforcement
Name Plains Pipeline, L.p.
Operator Street Address 333 Clay Street, Suite 1900
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-09-11 09:15:00
Location Latitude 32.0126 Google Maps OpenStreetMap
Location Longitude -102.02798 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-09-11 09:15:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-09-11 09:15:00
Restart Datetime 2015-09-14 13:00:00
On Site Datetime 2015-09-11 09:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Midland (Iraan) Terminal
Segment Name Sunrise To Midland 16"
Onshore State Abbreviation Tx
Onshore Postal Code 79706
Onshore City Name Midland
Onshore County Name Midland
Designated Location Milepost/valve Station
Designated Name 1.22
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Other
Item Involved Details Insulating Gasket
Installation Year 2015
Material Involved Material Other Than Carbon Steel
Material Details Phenolic Material
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 6900
Est Cost Emergency 1600
Est Cost Environmental 0
Est Cost Other 0
Prpty 8600
Accident Psig 637
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Installation Ind Yes
Preparer Name C******* C*****
Preparer Title Compliance Specialist
Preparer Email C*******@p****.com
Preparer Telephone 713-993-5080
Preparer Fax 713-646-4310
Prepared Date 2015-10-09 00:00:00
Authorizer Name T***** M*****
Authorizer Telephone 713-646-4109
Authorizer Title Sr Dir Of Environmental And Regulatory Compliance
Authorizer Email T*******@p****.com
Narrative Approximately 2 bbls of crude oil were released as a result of two failed insulator gaskets. The cause of the release was determined to be improper installation during construction. Both gaskets were replaced with a different type of gasket and verified for proper working condition. In addition, plains operators verified all gaskets were properly torqued. Furthermore, plains created a notification and awareness report (nar), to be sent to all relevant employees in order to help prevent reoccurrence.

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