HL incident on 2015-08-25 — OK

Operator
Chaparral Energy, Llc
Cause
Corrosion Failure
Commodity
Co2 (Carbon Dioxide)
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,000
Incident datetime
2015-08-25 09:55
Report number
Location
OK
Narrative
At approximately 0900 hrs on august 25th, chaparral received a call from a landowner stating he observed a possible CO2 leak on sunday, august 23rd on the coffeyville CO2 pipeline. No contact was made to chaparral until tuesday, august 25th. At approximately 0955 hrs on august 25th, the pipeline supervisor verified the location of the leak. Mlbv 12 was closed at approximately 1155 hrs and mlbv 13 was closed at approximately 1235 hrs. The isolated segment was blown down at both valve locations (12&13) at approximately 1235 hrs. Emergency onecalls were made to excavate the affected pipe. On tuesday, august 25th the pipeline was excavated and the leak location identified. On wednesday, august 26th, the affected section of pipe was removed and replaced with new pipe. The affected segment of pipe was sent to a testing laboratory on thursday, august 27th for further analysis.
Detailed record list
Report Received Date
2015-09-22 00:00:00
Iyear
2015
Report Number
20150341
Supplemental Number
21018
Report Type
Supplemental Final
Operator Id
Name
Chaparral Energy, Llc
Operator Street Address
701 Cedar Lake Blvd
Operator City Name
Oklahoma City
Operator State Abbreviation
OK
Operator Postal Code
73114
Local Datetime
2015-08-25 10:35:00
Location Latitude
Location Longitude
Commodity Released Type
Co2 (Carbon Dioxide)
Unintentional Release Bbls
28
Intentional Release Bbls
1033
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2015-08-25 09:55:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Source Plant Was Offline At The Time Of The Accident.
On Site Datetime
2015-08-25 09:55:00
Nrc Rpt Datetime
2015-08-25 10:35:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Coffeyville Co2 Pipeline
Segment Name
F2269
Onshore State Abbreviation
Ok
Onshore Postal Code
74652
Onshore City Name
Not Within A Municipality
Onshore County Name
Osage
Designated Location
Milepost/valve Station
Designated Name
Mp 66
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
60
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8.625
Pipe Wall Thickness
0.22
Pipe Smys
65000
Pipe Specification
Api 5l X65
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Corinth Pipe Works S. A.
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
2013
Manufactured Year
2012
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
65
Est Cost Prop Damage
10000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
10065
Accident Psig
1120
Mop Psig
2220
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
107865
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Stray Current Corrosion Ind
Yes
Other Basis Ind
Yes
Corrosion Basis Details
Sme Review
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
2014
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Cp Annual Survey Year
2015
Prior Damage
Yes
Collected Data Ind
Yes
Geometry Recent Year
2013
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
C*** N D******
Preparer Title
Sr. Pipeline Compliance Specialist
Preparer Email
C***********@c**************.com
Preparer Telephone
405-426-4470
Prepared Date
2015-12-30 00:00:00
Authorizer Name
C**** C*******
Authorizer Telephone
405-426-4335
Authorizer Title
Pipeline Foreman
Authorizer Email
C*************@c**************.com
Narrative
At approximately 0900 hrs on august 25th, chaparral received a call from a landowner stating he observed a possible CO2 leak on sunday, august 23rd on the coffeyville CO2 pipeline. No contact was made to chaparral until tuesday, august 25th. At approximately 0955 hrs on august 25th, the pipeline supervisor verified the location of the leak. Mlbv 12 was closed at approximately 1155 hrs and mlbv 13 was closed at approximately 1235 hrs. The isolated segment was blown down at both valve locations (12&13) at approximately 1235 hrs. Emergency onecalls were made to excavate the affected pipe. On tuesday, august 25th the pipeline was excavated and the leak location identified. On wednesday, august 26th, the affected section of pipe was removed and replaced with new pipe. The affected segment of pipe was sent to a testing laboratory on thursday, august 27th for further analysis.
Report Received Date 2015-09-22 00:00:00
Iyear 2015
Report Number 20150341
Supplemental Number 21018
Report Type Supplemental Final
Operator Id 31672 PHMSA Enforcement
Name Chaparral Energy, Llc
Operator Street Address 701 Cedar Lake Blvd
Operator City Name Oklahoma City
Operator State Abbreviation OK
Operator Postal Code 73114
Local Datetime 2015-08-25 10:35:00
Location Latitude 36.800991 Google Maps OpenStreetMap
Location Longitude -96.642259 Google Maps OpenStreetMap
Commodity Released Type Co2 (Carbon Dioxide)
Unintentional Release Bbls 28
Intentional Release Bbls 1033
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2015-08-25 09:55:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Source Plant Was Offline At The Time Of The Accident.
On Site Datetime 2015-08-25 09:55:00
Nrc Rpt Datetime 2015-08-25 10:35:00
Nrc Rpt Num 1126631 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Coffeyville Co2 Pipeline
Segment Name F2269
Onshore State Abbreviation Ok
Onshore Postal Code 74652
Onshore City Name Not Within A Municipality
Onshore County Name Osage
Designated Location Milepost/valve Station
Designated Name Mp 66
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 60
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8.625
Pipe Wall Thickness 0.22
Pipe Smys 65000
Pipe Specification Api 5l X65
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Corinth Pipe Works S. A.
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year 2013
Manufactured Year 2012
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 65
Est Cost Prop Damage 10000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 10065
Accident Psig 1120
Mop Psig 2220
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 107865
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Stray Current Corrosion Ind Yes
Other Basis Ind Yes
Corrosion Basis Details Sme Review
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 2014
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Cp Annual Survey Year 2015
Prior Damage Yes
Collected Data Ind Yes
Geometry Recent Year 2013
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name C*** N D******
Preparer Title Sr. Pipeline Compliance Specialist
Preparer Email C***********@c**************.com
Preparer Telephone 405-426-4470
Prepared Date 2015-12-30 00:00:00
Authorizer Name C**** C*******
Authorizer Telephone 405-426-4335
Authorizer Title Pipeline Foreman
Authorizer Email C*************@c**************.com
Narrative At approximately 0900 hrs on august 25th, chaparral received a call from a landowner stating he observed a possible CO2 leak on sunday, august 23rd on the coffeyville CO2 pipeline. No contact was made to chaparral until tuesday, august 25th. At approximately 0955 hrs on august 25th, the pipeline supervisor verified the location of the leak. Mlbv 12 was closed at approximately 1155 hrs and mlbv 13 was closed at approximately 1235 hrs. The isolated segment was blown down at both valve locations (12&13) at approximately 1235 hrs. Emergency onecalls were made to excavate the affected pipe. On tuesday, august 25th the pipeline was excavated and the leak location identified. On wednesday, august 26th, the affected section of pipe was removed and replaced with new pipe. The affected segment of pipe was sent to a testing laboratory on thursday, august 27th for further analysis.

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