HL incident on 2015-08-25 — TX

Operator
West Coast Terminal Pipeline (Wctp)
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$300
Incident datetime
2015-08-25 14:50
Report number
Location
TX
Narrative
On 08/25/15, a jet fuel release 31 gallons /0.74 bbls was discovered within the willbridge, or terminal (operator wctp). The release resulted from overfilling a 'gammon pot' (sump separator) associated with the water draw system of a jet fuel breakout tank. The breakout tank is used to transfer product to the portland airport via ls 1880. The immediate cause of the release was an internally leaking valve. Note: part (c) (4): facility was purchased in 1995. There are no records showing the date the valve was installed.
Detailed record list
Report Received Date
2015-09-21 00:00:00
Iyear
2015
Report Number
20150337
Supplemental Number
20756
Report Type
Original Final
Operator Id
Name
West Coast Terminal Pipeline (Wctp)
Operator Street Address
1001 Louisiana St., Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-08-25 11:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.74
Recovered Bbls
0.74
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-08-25 14:50:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline/facility Not Affected.
On Site Datetime
2015-08-25 14:50:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Willbridge Terminal
Segment Name
Willbridge Terminal
Onshore State Abbreviation
Or
Onshore Postal Code
97210
Onshore City Name
Portland
Onshore County Name
Multnomah
Designated Location
Survey Station No.
Designated Name
Willbridge Te
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Gammon Pot (Sump/separator)
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Sump
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
42
Est Cost Prop Damage
300
Est Cost Emergency
6000
Est Cost Environmental
2000
Est Cost Other
0
Prpty
8342
Accident Psig
15.5
Mop Psig
15.5
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Other Control Relief Ind
Yes
Other Control Relief Details
Internally Leaking Gate Valve Caused Gammon Pot (Sump/separator) Overfill.
Eq Additional Other Ind
Yes
Eq Additional Other Details
Soft Goods Failure Allowing Internal Leak Through Valve Causing Overfill.
Preparer Name
S**** M*******
Preparer Title
Mgr-Ccs
Preparer Email
S*************@k***********.com
Preparer Telephone
9098735146
Preparer Fax
3039843620
Prepared Date
2015-09-21 00:00:00
Authorizer Name
E***** A* F***
Authorizer Telephone
7133699454
Authorizer Title
Dir-Ccs
Authorizer Email
B********@k***********.com
Narrative
On 08/25/15, a jet fuel release 31 gallons /0.74 bbls was discovered within the willbridge, or terminal (operator wctp). The release resulted from overfilling a 'gammon pot' (sump separator) associated with the water draw system of a jet fuel breakout tank. The breakout tank is used to transfer product to the portland airport via ls 1880. The immediate cause of the release was an internally leaking valve. Note: part (c) (4): facility was purchased in 1995. There are no records showing the date the valve was installed.
Report Received Date 2015-09-21 00:00:00
Iyear 2015
Report Number 20150337
Supplemental Number 20756
Report Type Original Final
Operator Id 32688 PHMSA Enforcement
Name West Coast Terminal Pipeline (Wctp)
Operator Street Address 1001 Louisiana St., Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-08-25 11:00:00
Location Latitude 45.56545 Google Maps OpenStreetMap
Location Longitude -122.743195 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.74
Recovered Bbls 0.74
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-08-25 14:50:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline/facility Not Affected.
On Site Datetime 2015-08-25 14:50:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Willbridge Terminal
Segment Name Willbridge Terminal
Onshore State Abbreviation Or
Onshore Postal Code 97210
Onshore City Name Portland
Onshore County Name Multnomah
Designated Location Survey Station No.
Designated Name Willbridge Te
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Other
Incident Area Details Gammon Pot (Sump/separator)
Crossing No
Pipe Facility Type Interstate
Item Involved Sump
Installation Year Unknown
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 42
Est Cost Prop Damage 300
Est Cost Emergency 6000
Est Cost Environmental 2000
Est Cost Other 0
Prpty 8342
Accident Psig 15.5
Mop Psig 15.5
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Other Control Relief Ind Yes
Other Control Relief Details Internally Leaking Gate Valve Caused Gammon Pot (Sump/separator) Overfill.
Eq Additional Other Ind Yes
Eq Additional Other Details Soft Goods Failure Allowing Internal Leak Through Valve Causing Overfill.
Preparer Name S**** M*******
Preparer Title Mgr-Ccs
Preparer Email S*************@k***********.com
Preparer Telephone 9098735146
Preparer Fax 3039843620
Prepared Date 2015-09-21 00:00:00
Authorizer Name E***** A* F***
Authorizer Telephone 7133699454
Authorizer Title Dir-Ccs
Authorizer Email B********@k***********.com
Narrative On 08/25/15, a jet fuel release 31 gallons /0.74 bbls was discovered within the willbridge, or terminal (operator wctp). The release resulted from overfilling a 'gammon pot' (sump separator) associated with the water draw system of a jet fuel breakout tank. The breakout tank is used to transfer product to the portland airport via ls 1880. The immediate cause of the release was an internally leaking valve. Note: part (c) (4): facility was purchased in 1995. There are no records showing the date the valve was installed.

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