HL incident on 2015-08-27 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$363,545
Incident datetime
2015-08-27 17:30
Report number
Location
TX
Narrative
On 8/27/15 at approximately 17:30 local operations found crude oil seeping from the ground in manifold 200. The manifold was isolated and the source of the leak was identified to be a 2" stripping line. After excavation it was determined to be a pinhole leak at the 6 o'clock position due to internal corrosion. A plidco clamp was applied and line was placed back into service. Report has been updated with final repair cost.
Detailed record list
Report Received Date
2015-09-21 00:00:00
Iyear
2015
Report Number
20150336
Supplemental Number
21056
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-08-27 17:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
5
Recovered Bbls
3.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-08-27 17:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-08-27 17:30:00
Restart Datetime
2015-09-05 21:35:00
On Site Datetime
2015-08-27 17:30:00
Nrc Rpt Datetime
2015-08-27 17:35:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Hsc
Segment Name
Manifold 200
Onshore State Abbreviation
Tx
Onshore Postal Code
77015
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Hsc
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
72
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1600
Est Cost Prop Damage
363545
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
365145
Accident Psig
15
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller and control room were not a contributing factor.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Not Cut Open
Int Water Acid Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Preparer Name
C**** A******
Preparer Email
C*******@e****.com
Preparer Telephone
713-381-6426
Prepared Date
2016-01-19 00:00:00
Authorizer Name
C**** A******
Authorizer Telephone
713-381-6426
Authorizer Title
Pipeline Compliance Specialist
Authorizer Email
C*******@e****.com
Narrative
On 8/27/15 at approximately 17:30 local operations found crude oil seeping from the ground in manifold 200. The manifold was isolated and the source of the leak was identified to be a 2" stripping line. After excavation it was determined to be a pinhole leak at the 6 o'clock position due to internal corrosion. A plidco clamp was applied and line was placed back into service. Report has been updated with final repair cost.
Report Received Date 2015-09-21 00:00:00
Iyear 2015
Report Number 20150336
Supplemental Number 21056
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-08-27 17:30:00
Location Latitude 29.747453 Google Maps OpenStreetMap
Location Longitude -95.127678 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 5
Recovered Bbls 3.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-08-27 17:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-08-27 17:30:00
Restart Datetime 2015-09-05 21:35:00
On Site Datetime 2015-08-27 17:30:00
Nrc Rpt Datetime 2015-08-27 17:35:00
Nrc Rpt Num 1126868 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Hsc
Segment Name Manifold 200
Onshore State Abbreviation Tx
Onshore Postal Code 77015
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Hsc
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 72
Crossing No
Pipe Facility Type Intrastate
Item Involved Auxiliary Piping (E.g. Drain Lines)
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 1600
Est Cost Prop Damage 363545
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 365145
Accident Psig 15
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller and control room were not a contributing factor.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Not Cut Open
Int Water Acid Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Preparer Name C**** A******
Preparer Email C*******@e****.com
Preparer Telephone 713-381-6426
Prepared Date 2016-01-19 00:00:00
Authorizer Name C**** A******
Authorizer Telephone 713-381-6426
Authorizer Title Pipeline Compliance Specialist
Authorizer Email C*******@e****.com
Narrative On 8/27/15 at approximately 17:30 local operations found crude oil seeping from the ground in manifold 200. The manifold was isolated and the source of the leak was identified to be a 2" stripping line. After excavation it was determined to be a pinhole leak at the 6 o'clock position due to internal corrosion. A plidco clamp was applied and line was placed back into service. Report has been updated with final repair cost.

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