Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2015-08-27 — TX
Operator
Enterprise Crude Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$363,545
Incident datetime
2015-08-27 17:30
Report number
Location
TX
Narrative
On 8/27/15 at approximately 17:30 local operations found crude oil seeping from the ground in manifold 200. The manifold was isolated and the source of the leak was identified to be a 2" stripping line. After excavation it was determined to be a pinhole leak at the 6 o'clock position due to internal corrosion. A plidco clamp was applied and line was placed back into service. Report has been updated with final repair cost.
Detailed record list
Report Received Date
2015-09-21 00:00:00
Iyear
2015
Report Number
20150336
Supplemental Number
21056
Report Type
Supplemental Final
Operator Id
30829
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-08-27 17:30:00
Location Latitude
29.747453
Location Longitude
-95.127678
Commodity Released Type
Crude Oil
Unintentional Release Bbls
5
Recovered Bbls
3.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-08-27 17:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-08-27 17:30:00
Restart Datetime
2015-09-05 21:35:00
On Site Datetime
2015-08-27 17:30:00
Nrc Rpt Datetime
2015-08-27 17:35:00
Nrc Rpt Num
1126868
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Hsc
Segment Name
Manifold 200
Onshore State Abbreviation
Tx
Onshore Postal Code
77015
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Hsc
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
72
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
1600
Est Cost Prop Damage
363545
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
365145
Accident Psig
15
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller and control room were not a contributing factor.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Not Cut Open
Int Water Acid Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Preparer Name
C**** A******
Preparer Email
C*******@e****.com
Preparer Telephone
713-381-6426
Prepared Date
2016-01-19 00:00:00
Authorizer Name
C**** A******
Authorizer Telephone
713-381-6426
Authorizer Title
Pipeline Compliance Specialist
Authorizer Email
C*******@e****.com
Narrative
On 8/27/15 at approximately 17:30 local operations found crude oil seeping from the ground in manifold 200. The manifold was isolated and the source of the leak was identified to be a 2" stripping line. After excavation it was determined to be a pinhole leak at the 6 o'clock position due to internal corrosion. A plidco clamp was applied and line was placed back into service. Report has been updated with final repair cost.
| Report Received Date | 2015-09-21 00:00:00 |
|---|---|
| Iyear | 2015 |
| Report Number | 20150336 |
| Supplemental Number | 21056 |
| Report Type | Supplemental Final |
| Operator Id | 30829 PHMSA Enforcement |
| Name | Enterprise Crude Pipeline Llc |
| Operator Street Address | 1100 Louisiana Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2015-08-27 17:30:00 |
| Location Latitude | 29.747453 Google Maps OpenStreetMap |
| Location Longitude | -95.127678 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 5 |
| Recovered Bbls | 3.5 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2015-08-27 17:30:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2015-08-27 17:30:00 |
| Restart Datetime | 2015-09-05 21:35:00 |
| On Site Datetime | 2015-08-27 17:30:00 |
| Nrc Rpt Datetime | 2015-08-27 17:35:00 |
| Nrc Rpt Num | 1126868 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Hsc |
| Segment Name | Manifold 200 |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77015 |
| Onshore City Name | Houston |
| Onshore County Name | Harris |
| Designated Location | Milepost/valve Station |
| Designated Name | Hsc |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Soil |
| Depth Of Cover | 72 |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Auxiliary Piping (E.g. Drain Lines) |
| Installation Year | Unknown |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Pinhole |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 1600 |
| Est Cost Prop Damage | 363545 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 365145 |
| Accident Psig | 15 |
| Mop Psig | 275 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Controller and control room were not a contributing factor. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Corrosion Failure |
| Cause Details | Internal Corrosion |
| Internal External | Internal Corrosion |
| Int Visual Exam Results | Not Cut Open |
| Int Water Acid Ind | Yes |
| Int Field Exam Basis Ind | Yes |
| Int Low Point Pipe Loc Ind | Yes |
| Corrosion Inhibitors | No |
| Corrosion Lining | No |
| Cleaning Dewatering | Not Applicable - Not Mainline Pipe |
| Corrosion Coupons | Not Applicable - Not Mainline Pipe |
| Preparer Name | C**** A****** |
| Preparer Email | C*******@e****.com |
| Preparer Telephone | 713-381-6426 |
| Prepared Date | 2016-01-19 00:00:00 |
| Authorizer Name | C**** A****** |
| Authorizer Telephone | 713-381-6426 |
| Authorizer Title | Pipeline Compliance Specialist |
| Authorizer Email | C*******@e****.com |
| Narrative | On 8/27/15 at approximately 17:30 local operations found crude oil seeping from the ground in manifold 200. The manifold was isolated and the source of the leak was identified to be a 2" stripping line. After excavation it was determined to be a pinhole leak at the 6 o'clock position due to internal corrosion. A plidco clamp was applied and line was placed back into service. Report has been updated with final repair cost. |
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