HL incident on 2015-08-21 — TX

Operator
Sunoco Pipeline L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$14,000
Incident datetime
2015-08-21 17:00
Report number
Location
TX
Narrative
On 8/21/2015 a landowner notified sour lake field office of a stain on his property. Operations personnel responded, excavated the area and confirmed a pinhole leak on the nome to daniel's jct. 4" line segment. Approximately one barrel was released. The affected section of piping has been removed and replaced with new pipe. Chemical analysis of the affected piping revealed microbial induced corrosion (mic).
Detailed record list
Report Received Date
2015-09-18 00:00:00
Iyear
2015
Report Number
20150335
Supplemental Number
20926
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-08-21 17:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2015-08-21 17:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Excavated And A Plidco Clamp Installed.
On Site Datetime
2015-08-21 17:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Nome To Daniel's Jct. 4"
Segment Name
613006-4" Nome To Daniel's Jct.
Onshore State Abbreviation
Tx
Onshore Postal Code
77629
Onshore City Name
Nome
Onshore County Name
Jefferson
Designated Location
Survey Station No.
Designated Name
368+03
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
24
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
4.5
Pipe Wall Thickness
0.156
Pipe Smys
24000
Pipe Specification
Grade A
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1960
Manufactured Year
1960
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
14000
Est Cost Emergency
8000
Est Cost Environmental
0
Est Cost Other
0
Prpty
22000
Accident Psig
290
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
41712
Internal Inspection Ind
No
Diameter Change Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Other Basis Ind
Yes
Int Corrosion Basis Details
Chemical Analysis By Vendor.
Int Other Loc Ind
Yes
Corrosion Location Details
5 O'clock Position
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Yes
Corrosion Coupons
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2001
Hydrtst Most Rcnt Pressure
1033
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2015-11-23 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
On 8/21/2015 a landowner notified sour lake field office of a stain on his property. Operations personnel responded, excavated the area and confirmed a pinhole leak on the nome to daniel's jct. 4" line segment. Approximately one barrel was released. The affected section of piping has been removed and replaced with new pipe. Chemical analysis of the affected piping revealed microbial induced corrosion (mic).
Report Received Date 2015-09-18 00:00:00
Iyear 2015
Report Number 20150335
Supplemental Number 20926
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-08-21 17:00:00
Location Latitude 30.08493 Google Maps OpenStreetMap
Location Longitude -94.44736 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2015-08-21 17:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Excavated And A Plidco Clamp Installed.
On Site Datetime 2015-08-21 17:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Nome To Daniel's Jct. 4"
Segment Name 613006-4" Nome To Daniel's Jct.
Onshore State Abbreviation Tx
Onshore Postal Code 77629
Onshore City Name Nome
Onshore County Name Jefferson
Designated Location Survey Station No.
Designated Name 368+03
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 24
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 4.5
Pipe Wall Thickness 0.156
Pipe Smys 24000
Pipe Specification Grade A
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1960
Manufactured Year 1960
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 14000
Est Cost Emergency 8000
Est Cost Environmental 0
Est Cost Other 0
Prpty 22000
Accident Psig 290
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 41712
Internal Inspection Ind No
Diameter Change Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Other Basis Ind Yes
Int Corrosion Basis Details Chemical Analysis By Vendor.
Int Other Loc Ind Yes
Corrosion Location Details 5 O'clock Position
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Yes
Corrosion Coupons Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2001
Hydrtst Most Rcnt Pressure 1033
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2015-11-23 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative On 8/21/2015 a landowner notified sour lake field office of a stain on his property. Operations personnel responded, excavated the area and confirmed a pinhole leak on the nome to daniel's jct. 4" line segment. Approximately one barrel was released. The affected section of piping has been removed and replaced with new pipe. Chemical analysis of the affected piping revealed microbial induced corrosion (mic).

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