HL incident on 2015-08-21 — OK

Operator
Oneok Ngl Pipeline, Llc
Cause
Corrosion Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$55,000
Incident datetime
2015-08-21 13:14
Report number
Location
OK
Narrative
On august 21, 2015 oneok contractor sandblasting the #1 10" pipeline out of coahoma storage to verify an anomoly indicated by ili data, noticed hydrocarbon vapors coming from the pipe at the 12 o'clock position. Prior to the work, the excavation had been inspected and was clear of hydrocarbons. The oneok inspector confirmed hydrocarbon release on the pipeline at 13:18 hrs., inspector contacted pipeline control center and the pipeline supervisor. The pipeline was shutdown at 13:20 hrs. On 8/21/2015. Work to install a temporary clamp bgan and the release was contained by 15:45 hrs.. Oneok then displaced the hydrocarbons in the pipeline with nitrogen and 2 joints (approximately 80 ft.) of pipe were replaced at the location. Upon completion of the pipe replacement, the pipeline was returned to normal operation at approximately 11:35 hrs. On 8/23/2015. Corrected pipe specs to API 5l - 3/08/2016.
Detailed record list
Report Received Date
2015-09-18 00:00:00
Iyear
2015
Report Number
20150334
Supplemental Number
21206
Report Type
Supplemental
Operator Id
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2015-08-21 13:14:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.07
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-08-21 13:14:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-08-21 13:20:00
Restart Datetime
2015-08-23 11:35:00
On Site Datetime
2015-08-21 13:14:00
Nrc Rpt Datetime
2015-08-21 14:47:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Oneok Txl0415c Coahoma #1 10"
Segment Name
West Texas Lpg Index 23415
Onshore State Abbreviation
Tx
Onshore Postal Code
79511
Onshore City Name
Not Within A Municipality
Onshore County Name
Mitchell
Designated Location
Milepost/valve Station
Designated Name
8009+17
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
18
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10.75
Pipe Wall Thickness
0.365
Pipe Smys
35000
Pipe Specification
Api 5l
Pipe Seam Type
Seamless
Pipe Manufacturer
National Steel
Pipe Coating Type
None
Installation Year
1945
Manufactured Year
1945
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
3
Est Cost Prop Damage
55000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
55003
Accident Psig
635
Mop Psig
1000
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
50017
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No contoller actions were involved.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Galvanic Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1981
Shielding Evident
No
Cathodic Survey Type
Yes
Other Cp Survey Ind
Yes
Other Cp Survey Year
2013
Prior Damage
No
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2015
Geometry Recent Year
2015
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1972
Hydrtst Most Rcnt Pressure
1250
Direct Asmnt Conducted
Yes, And An Investigative Dig Was Cunducted At The Point Of The Accident
Direct Asmnt At Pnt Accdnt Yr
2015
Non Destructive Exam Ind
No
Preparer Name
N*** J****
Preparer Title
Regulatory Compliance Coordinator
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2016-03-08 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Coordinator
Authorizer Email
N*********@o****.com
Narrative
On august 21, 2015 oneok contractor sandblasting the #1 10" pipeline out of coahoma storage to verify an anomoly indicated by ili data, noticed hydrocarbon vapors coming from the pipe at the 12 o'clock position. Prior to the work, the excavation had been inspected and was clear of hydrocarbons. The oneok inspector confirmed hydrocarbon release on the pipeline at 13:18 hrs., inspector contacted pipeline control center and the pipeline supervisor. The pipeline was shutdown at 13:20 hrs. On 8/21/2015. Work to install a temporary clamp bgan and the release was contained by 15:45 hrs.. Oneok then displaced the hydrocarbons in the pipeline with nitrogen and 2 joints (approximately 80 ft.) of pipe were replaced at the location. Upon completion of the pipe replacement, the pipeline was returned to normal operation at approximately 11:35 hrs. On 8/23/2015. Corrected pipe specs to API 5l - 3/08/2016.
Report Received Date 2015-09-18 00:00:00
Iyear 2015
Report Number 20150334
Supplemental Number 21206
Report Type Supplemental
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2015-08-21 13:14:00
Location Latitude 32.285819 Google Maps OpenStreetMap
Location Longitude -101.168947 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.07
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-08-21 13:14:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-08-21 13:20:00
Restart Datetime 2015-08-23 11:35:00
On Site Datetime 2015-08-21 13:14:00
Nrc Rpt Datetime 2015-08-21 14:47:00
Nrc Rpt Num 1126316 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Oneok Txl0415c Coahoma #1 10"
Segment Name West Texas Lpg Index 23415
Onshore State Abbreviation Tx
Onshore Postal Code 79511
Onshore City Name Not Within A Municipality
Onshore County Name Mitchell
Designated Location Milepost/valve Station
Designated Name 8009+17
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 18
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10.75
Pipe Wall Thickness 0.365
Pipe Smys 35000
Pipe Specification Api 5l
Pipe Seam Type Seamless
Pipe Manufacturer National Steel
Pipe Coating Type None
Installation Year 1945
Manufactured Year 1945
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 3
Est Cost Prop Damage 55000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 55003
Accident Psig 635
Mop Psig 1000
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 50017
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No contoller actions were involved.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Galvanic Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1981
Shielding Evident No
Cathodic Survey Type Yes
Other Cp Survey Ind Yes
Other Cp Survey Year 2013
Prior Damage No
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2015
Geometry Recent Year 2015
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1972
Hydrtst Most Rcnt Pressure 1250
Direct Asmnt Conducted Yes, And An Investigative Dig Was Cunducted At The Point Of The Accident
Direct Asmnt At Pnt Accdnt Yr 2015
Non Destructive Exam Ind No
Preparer Name N*** J****
Preparer Title Regulatory Compliance Coordinator
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2933
Prepared Date 2016-03-08 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Regulatory Compliance Coordinator
Authorizer Email N*********@o****.com
Narrative On august 21, 2015 oneok contractor sandblasting the #1 10" pipeline out of coahoma storage to verify an anomoly indicated by ili data, noticed hydrocarbon vapors coming from the pipe at the 12 o'clock position. Prior to the work, the excavation had been inspected and was clear of hydrocarbons. The oneok inspector confirmed hydrocarbon release on the pipeline at 13:18 hrs., inspector contacted pipeline control center and the pipeline supervisor. The pipeline was shutdown at 13:20 hrs. On 8/21/2015. Work to install a temporary clamp bgan and the release was contained by 15:45 hrs.. Oneok then displaced the hydrocarbons in the pipeline with nitrogen and 2 joints (approximately 80 ft.) of pipe were replaced at the location. Upon completion of the pipe replacement, the pipeline was returned to normal operation at approximately 11:35 hrs. On 8/23/2015. Corrected pipe specs to API 5l - 3/08/2016.

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