HL incident on 2015-08-15 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$12,046
Incident datetime
2015-08-15 10:23
Report number
Location
TX
Narrative
On august 15, 2015 at approximately 10:23 am, an enbridge contractor reported approximately 30 gallons of crude oil in the area of the small diameter piping of valve 222-sv-15 near tank 15 in the superior terminal. The edmonton control center was contacted and tank 15 was isolated. A pipeline maintenance crew was dispatched to determine the source of the leak. It was discovered that the nipple on the lower body block and bleed was cracked at the point it enters into the valve body. The nipple was removed and a plug was installed later that afternoon and the line turned back over to the control center. The internal incident investigation discovered that the threads were cracked at the time of installation due to applying uneven force while threading the nipple into the valve body. The lower body block and bleed assembly will be replaced by year end. Approximately 130 cubic yards of contaminated soil was hauled to an approved disposal site.
Detailed record list
Report Received Date
2015-09-14 00:00:00
Iyear
2015
Report Number
20150327
Supplemental Number
20739
Report Type
Original Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2015-08-15 10:23:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.71
Recovered Bbls
0.71
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2015-08-15 10:23:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Was Isolated To Perform Cleanup And Repairs
On Site Datetime
2015-08-15 10:23:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Superior Terminal Tank 15
Segment Name
222-V-Sv15
Onshore State Abbreviation
Wi
Onshore Postal Code
54880
Onshore City Name
Superior
Onshore County Name
Douglas
Designated Location
Milepost/valve Station
Designated Name
Superior Term
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
216
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2010
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
31
Est Cost Prop Damage
12046
Est Cost Emergency
810
Est Cost Environmental
15250
Est Cost Other
0
Prpty
28137
Accident Psig
15
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Field identified during hydrovac excavations
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Threaded Fitting
Additional Installation Ind
Yes
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Preparer Fax
715-394-1564
Prepared Date
2015-09-14 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Manager Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On august 15, 2015 at approximately 10:23 am, an enbridge contractor reported approximately 30 gallons of crude oil in the area of the small diameter piping of valve 222-sv-15 near tank 15 in the superior terminal. The edmonton control center was contacted and tank 15 was isolated. A pipeline maintenance crew was dispatched to determine the source of the leak. It was discovered that the nipple on the lower body block and bleed was cracked at the point it enters into the valve body. The nipple was removed and a plug was installed later that afternoon and the line turned back over to the control center. The internal incident investigation discovered that the threads were cracked at the time of installation due to applying uneven force while threading the nipple into the valve body. The lower body block and bleed assembly will be replaced by year end. Approximately 130 cubic yards of contaminated soil was hauled to an approved disposal site.
Report Received Date 2015-09-14 00:00:00
Iyear 2015
Report Number 20150327
Supplemental Number 20739
Report Type Original Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2015-08-15 10:23:00
Location Latitude 46.6869 Google Maps OpenStreetMap
Location Longitude -92.0645 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.71
Recovered Bbls 0.71
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2015-08-15 10:23:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank Was Isolated To Perform Cleanup And Repairs
On Site Datetime 2015-08-15 10:23:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Superior Terminal Tank 15
Segment Name 222-V-Sv15
Onshore State Abbreviation Wi
Onshore Postal Code 54880
Onshore City Name Superior
Onshore County Name Douglas
Designated Location Milepost/valve Station
Designated Name Superior Term
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 216
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2010
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 31
Est Cost Prop Damage 12046
Est Cost Emergency 810
Est Cost Environmental 15250
Est Cost Other 0
Prpty 28137
Accident Psig 15
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Field identified during hydrovac excavations
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Threaded Fitting
Additional Installation Ind Yes
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Preparer Fax 715-394-1564
Prepared Date 2015-09-14 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Manager Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On august 15, 2015 at approximately 10:23 am, an enbridge contractor reported approximately 30 gallons of crude oil in the area of the small diameter piping of valve 222-sv-15 near tank 15 in the superior terminal. The edmonton control center was contacted and tank 15 was isolated. A pipeline maintenance crew was dispatched to determine the source of the leak. It was discovered that the nipple on the lower body block and bleed was cracked at the point it enters into the valve body. The nipple was removed and a plug was installed later that afternoon and the line turned back over to the control center. The internal incident investigation discovered that the threads were cracked at the time of installation due to applying uneven force while threading the nipple into the valve body. The lower body block and bleed assembly will be replaced by year end. Approximately 130 cubic yards of contaminated soil was hauled to an approved disposal site.

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