HL incident on 2015-08-11 — CA

Operator
Kern Oil & Refining Co.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2015-08-11 18:50
Report number
Location
CA
Narrative
The pipeline was inactive at the time the leak was discovered. The line has been out of service since 2010. Crude oil was discovered coming up from the ground. Emergency responders called kern to determine if we had any pipelines in the area. Kern responded to assist and investigate and mitigate. The line was exposed and clamped within a matter of hours. Emergency response efforts were made to remove free liquids via vacuum truck. Further efforts to assess the pipe and begin soil remediation commenced the following morning and continued over the following days. All affected soil was removed. The line segment was isolated from any possible sources and potential tie-ins. Kern prepared and submitted for approval a plan to formally abandon the line. To date, investigation efforts have not revealed the cause of the release given the line was not in active service.
Detailed record list
Report Received Date
2015-09-10 00:00:00
Iyear
2015
Report Number
20150325
Supplemental Number
21840
Report Type
Supplemental Final
Operator Id
Name
Kern Oil & Refining Co.
Operator Street Address
7724 E. Panama Lane
Operator City Name
Bakersfield
Operator State Abbreviation
CA
Operator Postal Code
93307
Local Datetime
2015-08-11 15:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
5
Recovered Bbls
5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Emergency Responder
Incident Identified Datetime
2015-08-11 18:50:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Already Inactive At Time Of Release
On Site Datetime
2015-08-11 18:50:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Hilltop Gathering System
Segment Name
Hilltop 6"
Onshore State Abbreviation
Ca
Onshore Postal Code
93307
Onshore City Name
Bakersfield
Onshore County Name
Kern
Designated Location
Milepost/valve Station
Designated Name
Hilltop
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
72
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6
Pipe Wall Thickness
Unknown
Pipe Smys
Unknown
Pipe Specification
Schedule 40
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
None
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Approx. 1/2 Inch Hole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
No
Est Cost Oper Paid
1000
Est Cost Gas Released
0
Est Cost Prop Damage
500
Est Cost Emergency
2000
Est Cost Environmental
15000
Est Cost Other
0
Prpty
18500
Accident Psig
6
Mop Psig
60
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
Unknown
Internal Inspection Ind
No
Diameter Change Ind
Yes
Operation Complications Ind
Yes
Low Flow Ind
Yes
Pipeline Function
=< 20% Smys Regulated Gathering
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
General Corrosion
Galvanic Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
No
Shielding Evident
No
Cathodic Survey Type
No
Prior Damage
No
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
Yes, And An Investigative Dig Was Cunducted At The Point Of The Accident
Direct Asmnt At Pnt Accdnt Yr
2015
Non Destructive Exam Ind
No
Preparer Name
M****** H****
Preparer Title
Ehs Manager
Preparer Email
M*****@k******.com
Preparer Telephone
661-845-0761
Preparer Fax
661-845-3561
Prepared Date
2016-11-15 00:00:00
Authorizer Name
M****** H****
Authorizer Telephone
661-845-0761
Authorizer Title
Ehs Manager
Authorizer Email
M*****@k******.com
Narrative
The pipeline was inactive at the time the leak was discovered. The line has been out of service since 2010. Crude oil was discovered coming up from the ground. Emergency responders called kern to determine if we had any pipelines in the area. Kern responded to assist and investigate and mitigate. The line was exposed and clamped within a matter of hours. Emergency response efforts were made to remove free liquids via vacuum truck. Further efforts to assess the pipe and begin soil remediation commenced the following morning and continued over the following days. All affected soil was removed. The line segment was isolated from any possible sources and potential tie-ins. Kern prepared and submitted for approval a plan to formally abandon the line. To date, investigation efforts have not revealed the cause of the release given the line was not in active service.
Report Received Date 2015-09-10 00:00:00
Iyear 2015
Report Number 20150325
Supplemental Number 21840
Report Type Supplemental Final
Operator Id 30658 PHMSA Enforcement
Name Kern Oil & Refining Co.
Operator Street Address 7724 E. Panama Lane
Operator City Name Bakersfield
Operator State Abbreviation CA
Operator Postal Code 93307
Local Datetime 2015-08-11 15:00:00
Location Latitude 35.298901 Google Maps OpenStreetMap
Location Longitude -118.914063 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 5
Recovered Bbls 5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Emergency Responder
Incident Identified Datetime 2015-08-11 18:50:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Already Inactive At Time Of Release
On Site Datetime 2015-08-11 18:50:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Hilltop Gathering System
Segment Name Hilltop 6"
Onshore State Abbreviation Ca
Onshore Postal Code 93307
Onshore City Name Bakersfield
Onshore County Name Kern
Designated Location Milepost/valve Station
Designated Name Hilltop
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 72
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6
Pipe Wall Thickness Unknown
Pipe Smys Unknown
Pipe Specification Schedule 40
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer Unknown
Pipe Coating Type None
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Approx. 1/2 Inch Hole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No No
Est Cost Oper Paid 1000
Est Cost Gas Released 0
Est Cost Prop Damage 500
Est Cost Emergency 2000
Est Cost Environmental 15000
Est Cost Other 0
Prpty 18500
Accident Psig 6
Mop Psig 60
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated Unknown
Internal Inspection Ind No
Diameter Change Ind Yes
Operation Complications Ind Yes
Low Flow Ind Yes
Pipeline Function =< 20% Smys Regulated Gathering
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results General Corrosion
Galvanic Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind No
Shielding Evident No
Cathodic Survey Type No
Prior Damage No
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted Yes, And An Investigative Dig Was Cunducted At The Point Of The Accident
Direct Asmnt At Pnt Accdnt Yr 2015
Non Destructive Exam Ind No
Preparer Name M****** H****
Preparer Title Ehs Manager
Preparer Email M*****@k******.com
Preparer Telephone 661-845-0761
Preparer Fax 661-845-3561
Prepared Date 2016-11-15 00:00:00
Authorizer Name M****** H****
Authorizer Telephone 661-845-0761
Authorizer Title Ehs Manager
Authorizer Email M*****@k******.com
Narrative The pipeline was inactive at the time the leak was discovered. The line has been out of service since 2010. Crude oil was discovered coming up from the ground. Emergency responders called kern to determine if we had any pipelines in the area. Kern responded to assist and investigate and mitigate. The line was exposed and clamped within a matter of hours. Emergency response efforts were made to remove free liquids via vacuum truck. Further efforts to assess the pipe and begin soil remediation commenced the following morning and continued over the following days. All affected soil was removed. The line segment was isolated from any possible sources and potential tie-ins. Kern prepared and submitted for approval a plan to formally abandon the line. To date, investigation efforts have not revealed the cause of the release given the line was not in active service.

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