HL incident on 2015-08-24 — OH

Operator
Marathon Pipe Line Llc
Cause
Other Accident Cause
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2015-08-24 09:30
Report number
Location
OH
Narrative
A small flash (1-2 inch high) fire under the tank floor occurred during 653 maintenance work on tank 1211 at martinsville. All procedures were followed properly. Lels were being monitored within inches of the torch cutting site before the flash fire and following the incident with no lels found. The fire self-extinguished immediately and a plan was developed to mitigate recurrence. Phmsa requested the "estimated volume of commodity unintentionally released" be update from 0 to the minimum amount of .1 barrels. To clarify, the flash fire ignited due to vapors rather than liquid product.
Detailed record list
Report Received Date
2015-09-10 00:00:00
Iyear
2015
Report Number
20150322
Supplemental Number
21037
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2015-08-24 09:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
0.1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2015-08-24 09:30:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Was Undergoing An Api 653 And Was Disconnected From The Pipeline System.
On Site Datetime
2015-08-24 09:30:00
Nrc Rpt Datetime
2015-08-24 11:17:00
Nrc Rpt Num
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Martinsville Station (North Products Station)
Segment Name
N/a, Tank Physically Disconnected From The System
Onshore State Abbreviation
Il
Onshore Postal Code
62442
Onshore City Name
Martinsville
Onshore County Name
Clark
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Single Bottom System
Tank Type
Atmospheric
Installation Year
1937
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
It Is Believed That The Flash Fire, Which Occurred During Torch Cutting, Was Due To Conditions Underneath And Outside The Tank.
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
0
Accident Psig
0
Mop Psig
0
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Miscellaneous
Other Type
Miscellaneous
Misc Details
It Is Believed That The Flash Fire, Which Occurred During Torch Cutting, Was Due To Conditions Underneath And Outside The Tank.
Preparer Name
D******* S***
Preparer Title
Hes Professional
Preparer Email
D*****@m****************.com
Preparer Telephone
419-421-2121
Prepared Date
2016-01-08 00:00:00
Authorizer Name
R****** W* B*****
Authorizer Telephone
419-421-2121
Authorizer Title
Regulatory And Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
A small flash (1-2 inch high) fire under the tank floor occurred during 653 maintenance work on tank 1211 at martinsville. All procedures were followed properly. Lels were being monitored within inches of the torch cutting site before the flash fire and following the incident with no lels found. The fire self-extinguished immediately and a plan was developed to mitigate recurrence. Phmsa requested the "estimated volume of commodity unintentionally released" be update from 0 to the minimum amount of .1 barrels. To clarify, the flash fire ignited due to vapors rather than liquid product.
Report Received Date 2015-09-10 00:00:00
Iyear 2015
Report Number 20150322
Supplemental Number 21037
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2015-08-24 09:30:00
Location Latitude 39.32604 Google Maps OpenStreetMap
Location Longitude -87.89748 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 0.1
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2015-08-24 09:30:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank Was Undergoing An Api 653 And Was Disconnected From The Pipeline System.
On Site Datetime 2015-08-24 09:30:00
Nrc Rpt Datetime 2015-08-24 11:17:00
Nrc Rpt Num 1126542 NRC Report How to search
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Martinsville Station (North Products Station)
Segment Name N/a, Tank Physically Disconnected From The System
Onshore State Abbreviation Il
Onshore Postal Code 62442
Onshore City Name Martinsville
Onshore County Name Clark
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Single Bottom System
Tank Type Atmospheric
Installation Year 1937
Material Involved Carbon Steel
Release Type Other
Release Type Details It Is Believed That The Flash Fire, Which Occurred During Torch Cutting, Was Due To Conditions Underneath And Outside The Tank.
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 0
Accident Psig 0
Mop Psig 0
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Miscellaneous
Other Type Miscellaneous
Misc Details It Is Believed That The Flash Fire, Which Occurred During Torch Cutting, Was Due To Conditions Underneath And Outside The Tank.
Preparer Name D******* S***
Preparer Title Hes Professional
Preparer Email D*****@m****************.com
Preparer Telephone 419-421-2121
Prepared Date 2016-01-08 00:00:00
Authorizer Name R****** W* B*****
Authorizer Telephone 419-421-2121
Authorizer Title Regulatory And Compliance Supervisor
Authorizer Email R*******@m****************.com
Narrative A small flash (1-2 inch high) fire under the tank floor occurred during 653 maintenance work on tank 1211 at martinsville. All procedures were followed properly. Lels were being monitored within inches of the torch cutting site before the flash fire and following the incident with no lels found. The fire self-extinguished immediately and a plan was developed to mitigate recurrence. Phmsa requested the "estimated volume of commodity unintentionally released" be update from 0 to the minimum amount of .1 barrels. To clarify, the flash fire ignited due to vapors rather than liquid product.

All rights reserved. Copyright © by ClearPHMSA