HL incident on 2015-08-12 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$6,000
Incident datetime
2015-08-12 09:24
Report number
Location
TX
Narrative
On 8/12/2015 at 09:22, an enterprise technician identified a release from the bonnet of a block valve within mclouth station. The station was shutdown at 20:40 after attempts to fix the valve while in-service were not successful. After the faulty valve was isolated, the blocked in section was purged with nitrogen and the valve was then repaired. The line was restarted on 8/13/2015 at 17:00.
Detailed record list
Report Received Date
2015-09-09 00:00:00
Iyear
2015
Report Number
20150321
Supplemental Number
21131
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-08-12 09:24:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethane/propane
Unintentional Release Bbls
3
Intentional Release Bbls
20
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-08-12 09:24:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-08-12 20:40:00
Restart Datetime
2015-08-13 17:00:00
On Site Datetime
2015-08-12 09:24:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Mclouth Station
Segment Name
600-601-602
Onshore State Abbreviation
Ks
Onshore Postal Code
66048
Onshore City Name
Leavenworth
Onshore County Name
Leavenworth County
Designated Location
Survey Station No.
Designated Name
824637
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
1960
Material Involved
Material Other Than Carbon Steel
Material Details
O-Ring
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
300
Est Cost Prop Damage
6000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
6300
Accident Psig
1300
Mop Psig
1650
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller and control room were not a contributing factor.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Block Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Wear And Tear
Preparer Name
R** L**
Preparer Title
Pipeline Compliance Engineer
Preparer Email
R***@e****.com
Preparer Telephone
713-381-6741
Prepared Date
2016-02-16 00:00:00
Authorizer Name
R** L**
Authorizer Telephone
713-381-6741
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
R***@e****.com
Narrative
On 8/12/2015 at 09:22, an enterprise technician identified a release from the bonnet of a block valve within mclouth station. The station was shutdown at 20:40 after attempts to fix the valve while in-service were not successful. After the faulty valve was isolated, the blocked in section was purged with nitrogen and the valve was then repaired. The line was restarted on 8/13/2015 at 17:00.
Report Received Date 2015-09-09 00:00:00
Iyear 2015
Report Number 20150321
Supplemental Number 21131
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-08-12 09:24:00
Location Latitude 39.173564 Google Maps OpenStreetMap
Location Longitude -95.209343 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethane/propane
Unintentional Release Bbls 3
Intentional Release Bbls 20
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-08-12 09:24:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-08-12 20:40:00
Restart Datetime 2015-08-13 17:00:00
On Site Datetime 2015-08-12 09:24:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Mclouth Station
Segment Name 600-601-602
Onshore State Abbreviation Ks
Onshore Postal Code 66048
Onshore City Name Leavenworth
Onshore County Name Leavenworth County
Designated Location Survey Station No.
Designated Name 824637
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 1960
Material Involved Material Other Than Carbon Steel
Material Details O-Ring
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 300
Est Cost Prop Damage 6000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 6300
Accident Psig 1300
Mop Psig 1650
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller and control room were not a contributing factor.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Block Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Wear And Tear
Preparer Name R** L**
Preparer Title Pipeline Compliance Engineer
Preparer Email R***@e****.com
Preparer Telephone 713-381-6741
Prepared Date 2016-02-16 00:00:00
Authorizer Name R** L**
Authorizer Telephone 713-381-6741
Authorizer Title Pipeline Compliance Engineer
Authorizer Email R***@e****.com
Narrative On 8/12/2015 at 09:22, an enterprise technician identified a release from the bonnet of a block valve within mclouth station. The station was shutdown at 20:40 after attempts to fix the valve while in-service were not successful. After the faulty valve was isolated, the blocked in section was purged with nitrogen and the valve was then repaired. The line was restarted on 8/13/2015 at 17:00.

All rights reserved. Copyright © by ClearPHMSA