HL incident on 2015-08-11 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25,539
Incident datetime
2015-08-11 17:31
Report number
Location
TX
Narrative
During normal butane delivery operations, a valve closed inside the total refinery. At the time, the pipeline was flowing through the prover loop. The pressure in the prover loop increased when total's valve closed. The pressure did not exceed the mop of the piping - the line operates at approximately half of its mop during normal operations. The pressure increase caused a gasket on the prover loop to fail. The prover loop was isolated and blown down, and all gaskets on the prover loop were replaced with gaskets of a more reliable design. The line was shut down until the prover had been blown down and it was safe for personnel to enter the area, at which time the prover was bypassed and normal deliveries to the total refinery resumed.
Detailed record list
Report Received Date
2015-09-08 00:00:00
Iyear
2015
Report Number
20150319
Supplemental Number
20799
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-08-11 17:28:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Butane
Unintentional Release Bbls
0.6
Intentional Release Bbls
25
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-08-11 17:31:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-08-11 17:31:00
Restart Datetime
2015-08-11 21:00:00
On Site Datetime
2015-08-11 17:31:00
Nrc Rpt Datetime
2015-08-11 18:35:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
P89 - Butane Mainline
Segment Name
Basf Valve Site
Onshore State Abbreviation
Tx
Onshore Postal Code
77642
Onshore City Name
Port Arthur
Onshore County Name
Jefferson
Designated Location
Survey Station No.
Designated Name
352370
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Meter/prover
Installation Year
2010
Material Involved
Material Other Than Carbon Steel
Material Details
Gasket On Prover
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
559
Est Cost Prop Damage
25539
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
26098
Accident Psig
770
Mop Psig
1330
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Proving is done locally, therefore controller and control room were not contributing factors.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Defect Ind
Yes
Preparer Name
M*** P*****
Preparer Title
Sr. Compliance Specialist
Preparer Email
M*******@e****.com
Preparer Telephone
713-381-5897
Prepared Date
2015-10-05 00:00:00
Authorizer Name
M*** P*****
Authorizer Telephone
713-381-5897
Authorizer Title
Sr. Compliance Specialist
Authorizer Email
M*******@e****.com
Narrative
During normal butane delivery operations, a valve closed inside the total refinery. At the time, the pipeline was flowing through the prover loop. The pressure in the prover loop increased when total's valve closed. The pressure did not exceed the mop of the piping - the line operates at approximately half of its mop during normal operations. The pressure increase caused a gasket on the prover loop to fail. The prover loop was isolated and blown down, and all gaskets on the prover loop were replaced with gaskets of a more reliable design. The line was shut down until the prover had been blown down and it was safe for personnel to enter the area, at which time the prover was bypassed and normal deliveries to the total refinery resumed.
Report Received Date 2015-09-08 00:00:00
Iyear 2015
Report Number 20150319
Supplemental Number 20799
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-08-11 17:28:00
Location Latitude 29.952028 Google Maps OpenStreetMap
Location Longitude -93.887943 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Butane
Unintentional Release Bbls 0.6
Intentional Release Bbls 25
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-08-11 17:31:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-08-11 17:31:00
Restart Datetime 2015-08-11 21:00:00
On Site Datetime 2015-08-11 17:31:00
Nrc Rpt Datetime 2015-08-11 18:35:00
Nrc Rpt Num 1125373 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name P89 - Butane Mainline
Segment Name Basf Valve Site
Onshore State Abbreviation Tx
Onshore Postal Code 77642
Onshore City Name Port Arthur
Onshore County Name Jefferson
Designated Location Survey Station No.
Designated Name 352370
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Meter/prover
Installation Year 2010
Material Involved Material Other Than Carbon Steel
Material Details Gasket On Prover
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 559
Est Cost Prop Damage 25539
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 26098
Accident Psig 770
Mop Psig 1330
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Proving is done locally, therefore controller and control room were not contributing factors.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Defect Ind Yes
Preparer Name M*** P*****
Preparer Title Sr. Compliance Specialist
Preparer Email M*******@e****.com
Preparer Telephone 713-381-5897
Prepared Date 2015-10-05 00:00:00
Authorizer Name M*** P*****
Authorizer Telephone 713-381-5897
Authorizer Title Sr. Compliance Specialist
Authorizer Email M*******@e****.com
Narrative During normal butane delivery operations, a valve closed inside the total refinery. At the time, the pipeline was flowing through the prover loop. The pressure in the prover loop increased when total's valve closed. The pressure did not exceed the mop of the piping - the line operates at approximately half of its mop during normal operations. The pressure increase caused a gasket on the prover loop to fail. The prover loop was isolated and blown down, and all gaskets on the prover loop were replaced with gaskets of a more reliable design. The line was shut down until the prover had been blown down and it was safe for personnel to enter the area, at which time the prover was bypassed and normal deliveries to the total refinery resumed.

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