HL incident on 2015-08-09 — OK

Operator
Williams Field Services
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$750
Incident datetime
2015-08-09 09:18
Report number
Location
OK
Narrative
8:14 a.M. Pipeline control received gas detection at pump station, station went into emergency shutdown. 9:18 a.M. Operations employee when about 3/4 of mile from site and noticed a vapor cloud in station approx 10 feet high by 8 feet wide drifting south, called pipeline control of event, secured road into station with red danger tape. 09:27 a.M. Declared it an emergency event and activated the emergency response plan, call 911 to get help securing access to road south of station. Set up incident command appointed ic and safety officer 09:35 a.M. Called es&h to notify them of release 9:42 a.M. Called pipeline control on status update of pressure 170 psi suction side, 917 discharge side check valve was holding and station valves were closed when gas detection shut station down. 10:35 a.M. Op/techs walked for a closer look, and found the strainer was leaking, vapor cloud had diminished. Did a plan to go into site and isolate strainer on inlet side 10:48 a.M. Closed strainer inlet valve, no flammable vapors detected during closure 10:53 a.M. Update of pressure at pc 166 psi 11:00 a.M. Blew down suction piping to knockout drum 11:18 a.M. Closed outlet valve of strainer. 11:27 a.M. Pipeline control saw a pressure of 133 psi 11:28 a.M. Closed blowdown valve of header and opened blowdown of strainer 11:58 a.M. Emergency event has been terminated. 12:00 p.M. Strainer is completely isolated and blown down 12:30 p.M. Opened the strainer and found the o-ring was broke cleaned the threads of enclosure 1:45 p.M. Closed up the strainer and waited for further instruction strainer is currently bypassed until further investigation has been completed.
Detailed record list
Report Received Date
2015-09-03 00:00:00
Iyear
2015
Report Number
20150317
Supplemental Number
20869
Report Type
Supplemental Final
Operator Id
Name
Williams Field Services
Operator Street Address
One Williams Center Wrc-3
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74172
Local Datetime
2015-08-09 08:14:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
93.85
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2015-08-09 09:18:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-08-09 08:14:00
Restart Datetime
2015-08-09 15:05:00
On Site Datetime
2015-08-09 09:18:00
Nrc Rpt Datetime
2015-08-09 12:19:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Overland Pass Pipeline
Segment Name
Ogallah Pump Station
Onshore State Abbreviation
Ks
Onshore Postal Code
67656
Onshore City Name
Ogallah
Onshore County Name
Trego
Designated Location
Milepost/valve Station
Designated Name
643
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Strainer
Installation Year
2009
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
5000
Est Cost Prop Damage
750
Est Cost Emergency
250
Est Cost Environmental
0
Est Cost Other
0
Prpty
6000
Accident Psig
575
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Release was due to an equipment o-ring failure, controller action not applicable.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Release Was Due To The Failure Of An O-Ring On The Station Inlet Strainer Yale End Cap.
Additional Installation Ind
Yes
Preparer Name
M****** V** H***
Preparer Title
Pipeline Safety Engineer
Preparer Email
M**************@w*******.com
Preparer Telephone
801-584-6931
Prepared Date
2015-11-02 00:00:00
Authorizer Name
J**** E********
Authorizer Telephone
801-584-6539
Authorizer Title
Pipeline Safety Manager
Authorizer Email
J**************@w*******.com
Narrative
8:14 a.M. Pipeline control received gas detection at pump station, station went into emergency shutdown. 9:18 a.M. Operations employee when about 3/4 of mile from site and noticed a vapor cloud in station approx 10 feet high by 8 feet wide drifting south, called pipeline control of event, secured road into station with red danger tape. 09:27 a.M. Declared it an emergency event and activated the emergency response plan, call 911 to get help securing access to road south of station. Set up incident command appointed ic and safety officer 09:35 a.M. Called es&h to notify them of release 9:42 a.M. Called pipeline control on status update of pressure 170 psi suction side, 917 discharge side check valve was holding and station valves were closed when gas detection shut station down. 10:35 a.M. Op/techs walked for a closer look, and found the strainer was leaking, vapor cloud had diminished. Did a plan to go into site and isolate strainer on inlet side 10:48 a.M. Closed strainer inlet valve, no flammable vapors detected during closure 10:53 a.M. Update of pressure at pc 166 psi 11:00 a.M. Blew down suction piping to knockout drum 11:18 a.M. Closed outlet valve of strainer. 11:27 a.M. Pipeline control saw a pressure of 133 psi 11:28 a.M. Closed blowdown valve of header and opened blowdown of strainer 11:58 a.M. Emergency event has been terminated. 12:00 p.M. Strainer is completely isolated and blown down 12:30 p.M. Opened the strainer and found the o-ring was broke cleaned the threads of enclosure 1:45 p.M. Closed up the strainer and waited for further instruction strainer is currently bypassed until further investigation has been completed.
Report Received Date 2015-09-03 00:00:00
Iyear 2015
Report Number 20150317
Supplemental Number 20869
Report Type Supplemental Final
Operator Id 30826 PHMSA Enforcement
Name Williams Field Services
Operator Street Address One Williams Center Wrc-3
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74172
Local Datetime 2015-08-09 08:14:00
Location Latitude 38.938778 Google Maps OpenStreetMap
Location Longitude -99.761363 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 93.85
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2015-08-09 09:18:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-08-09 08:14:00
Restart Datetime 2015-08-09 15:05:00
On Site Datetime 2015-08-09 09:18:00
Nrc Rpt Datetime 2015-08-09 12:19:00
Nrc Rpt Num 1125150 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Overland Pass Pipeline
Segment Name Ogallah Pump Station
Onshore State Abbreviation Ks
Onshore Postal Code 67656
Onshore City Name Ogallah
Onshore County Name Trego
Designated Location Milepost/valve Station
Designated Name 643
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Strainer
Installation Year 2009
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 5000
Est Cost Prop Damage 750
Est Cost Emergency 250
Est Cost Environmental 0
Est Cost Other 0
Prpty 6000
Accident Psig 575
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Release was due to an equipment o-ring failure, controller action not applicable.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Release Was Due To The Failure Of An O-Ring On The Station Inlet Strainer Yale End Cap.
Additional Installation Ind Yes
Preparer Name M****** V** H***
Preparer Title Pipeline Safety Engineer
Preparer Email M**************@w*******.com
Preparer Telephone 801-584-6931
Prepared Date 2015-11-02 00:00:00
Authorizer Name J**** E********
Authorizer Telephone 801-584-6539
Authorizer Title Pipeline Safety Manager
Authorizer Email J**************@w*******.com
Narrative 8:14 a.M. Pipeline control received gas detection at pump station, station went into emergency shutdown. 9:18 a.M. Operations employee when about 3/4 of mile from site and noticed a vapor cloud in station approx 10 feet high by 8 feet wide drifting south, called pipeline control of event, secured road into station with red danger tape. 09:27 a.M. Declared it an emergency event and activated the emergency response plan, call 911 to get help securing access to road south of station. Set up incident command appointed ic and safety officer 09:35 a.M. Called es&h to notify them of release 9:42 a.M. Called pipeline control on status update of pressure 170 psi suction side, 917 discharge side check valve was holding and station valves were closed when gas detection shut station down. 10:35 a.M. Op/techs walked for a closer look, and found the strainer was leaking, vapor cloud had diminished. Did a plan to go into site and isolate strainer on inlet side 10:48 a.M. Closed strainer inlet valve, no flammable vapors detected during closure 10:53 a.M. Update of pressure at pc 166 psi 11:00 a.M. Blew down suction piping to knockout drum 11:18 a.M. Closed outlet valve of strainer. 11:27 a.M. Pipeline control saw a pressure of 133 psi 11:28 a.M. Closed blowdown valve of header and opened blowdown of strainer 11:58 a.M. Emergency event has been terminated. 12:00 p.M. Strainer is completely isolated and blown down 12:30 p.M. Opened the strainer and found the o-ring was broke cleaned the threads of enclosure 1:45 p.M. Closed up the strainer and waited for further instruction strainer is currently bypassed until further investigation has been completed.

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