HL incident on 2015-08-02 — TX

Operator
Centurion Pipeline L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$26,589
Incident datetime
2015-08-02 07:55
Report number
Location
TX
Narrative
At approximately 08: 15 a.M. (central time) on august 2, 2015, a centurion employee observed that tank no. 6830 at the wasson station was leaking from the mixer. With assistance from the region manager, a vacuum truck was used to collect spilled oil. And the tank was pumped out to lower the oil level in the tank and all incoming flow of oil was blocked from artesia, nm. Communication with houston control room and centurion's asset integrity department was initiated. The volume spilled inside the tank dike was measured and found to be about 314 barrels at 10:30 a.M., so the spill was reported to the national response center by cutty cunningham at 10:30 am (central time). At 13:30 p.M. August 4, 2015, the mixer for tank no. 6830 was replaced and refilling the tank was commenced with incoming crude from artesia, nm
Detailed record list
Report Received Date
2015-08-31 00:00:00
Iyear
2015
Report Number
20150313
Supplemental Number
21603
Report Type
Supplemental Final
Operator Id
Name
Centurion Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-08-02 07:55:00
Location Latitude
Location Longitude
-102.7692504
Commodity Released Type
Crude Oil
Unintentional Release Bbls
321
Recovered Bbls
165
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2015-08-02 07:55:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-08-02 08:15:00
Restart Datetime
2015-08-04 13:30:00
On Site Datetime
2015-08-02 11:30:00
Nrc Rpt Datetime
2015-08-02 10:30:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Tank #6830
Segment Name
Artesia To Wasson
Onshore State Abbreviation
Tx
Onshore Postal Code
79323
Onshore City Name
Not Within A Municipality
Onshore County Name
Yoakum
Designated Location
Milepost/valve Station
Designated Name
Wasson Sta.
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Mixer
Tank Type
Atmospheric
Installation Year
2005
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Tank Mixer Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
2650
Est Cost Prop Damage
26589
Est Cost Emergency
3218
Est Cost Environmental
30000
Est Cost Other
0
Prpty
62457
Accident Psig
3
Mop Psig
14.7
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak not associated with operational functions of control room
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Seal And Bearings On Tank Mixer Failed.
Eq Additional Other Ind
Yes
Eq Additional Other Details
Seal On Mixer Equipment
Preparer Name
C**** C*********
Preparer Title
Manager Asset Integrity
Preparer Email
C***************@o**.com
Preparer Telephone
(713)497-2016
Preparer Fax
(713)215-7455
Prepared Date
2016-08-16 00:00:00
Authorizer Name
C**** C*********
Authorizer Telephone
(713)497-2016
Authorizer Title
Manager Asset Integrity
Authorizer Email
C***************@o**.com
Narrative
At approximately 08: 15 a.M. (central time) on august 2, 2015, a centurion employee observed that tank no. 6830 at the wasson station was leaking from the mixer. With assistance from the region manager, a vacuum truck was used to collect spilled oil. And the tank was pumped out to lower the oil level in the tank and all incoming flow of oil was blocked from artesia, nm. Communication with houston control room and centurion's asset integrity department was initiated. The volume spilled inside the tank dike was measured and found to be about 314 barrels at 10:30 a.M., so the spill was reported to the national response center by cutty cunningham at 10:30 am (central time). At 13:30 p.M. August 4, 2015, the mixer for tank no. 6830 was replaced and refilling the tank was commenced with incoming crude from artesia, nm
Report Received Date 2015-08-31 00:00:00
Iyear 2015
Report Number 20150313
Supplemental Number 21603
Report Type Supplemental Final
Operator Id 31888 PHMSA Enforcement
Name Centurion Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-08-02 07:55:00
Location Latitude 32.989666 Google Maps OpenStreetMap
Location Longitude -102.7692504 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 321
Recovered Bbls 165
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2015-08-02 07:55:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-08-02 08:15:00
Restart Datetime 2015-08-04 13:30:00
On Site Datetime 2015-08-02 11:30:00
Nrc Rpt Datetime 2015-08-02 10:30:00
Nrc Rpt Num 1124543 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Tank #6830
Segment Name Artesia To Wasson
Onshore State Abbreviation Tx
Onshore Postal Code 79323
Onshore City Name Not Within A Municipality
Onshore County Name Yoakum
Designated Location Milepost/valve Station
Designated Name Wasson Sta.
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Mixer
Tank Type Atmospheric
Installation Year 2005
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Tank Mixer Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 2650
Est Cost Prop Damage 26589
Est Cost Emergency 3218
Est Cost Environmental 30000
Est Cost Other 0
Prpty 62457
Accident Psig 3
Mop Psig 14.7
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak not associated with operational functions of control room
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Seal And Bearings On Tank Mixer Failed.
Eq Additional Other Ind Yes
Eq Additional Other Details Seal On Mixer Equipment
Preparer Name C**** C*********
Preparer Title Manager Asset Integrity
Preparer Email C***************@o**.com
Preparer Telephone (713)497-2016
Preparer Fax (713)215-7455
Prepared Date 2016-08-16 00:00:00
Authorizer Name C**** C*********
Authorizer Telephone (713)497-2016
Authorizer Title Manager Asset Integrity
Authorizer Email C***************@o**.com
Narrative At approximately 08: 15 a.M. (central time) on august 2, 2015, a centurion employee observed that tank no. 6830 at the wasson station was leaking from the mixer. With assistance from the region manager, a vacuum truck was used to collect spilled oil. And the tank was pumped out to lower the oil level in the tank and all incoming flow of oil was blocked from artesia, nm. Communication with houston control room and centurion's asset integrity department was initiated. The volume spilled inside the tank dike was measured and found to be about 314 barrels at 10:30 a.M., so the spill was reported to the national response center by cutty cunningham at 10:30 am (central time). At 13:30 p.M. August 4, 2015, the mixer for tank no. 6830 was replaced and refilling the tank was commenced with incoming crude from artesia, nm

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