HL incident on 2015-07-28 — PA

Operator
Buckeye Partners, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000
Incident datetime
2015-07-28 11:45
Report number
Location
PA
Narrative
Employee performing maintenance tasks had his air monitor alarmed with a high lel reading. The control center shutdown line 165 to isolate the section. A line probe was used down the side of the valve and it did not indicate any free product. Upon excavation product could be seen weeping from the valve stem. Packing was added to stop the leak and the contaminated soil was removed. All necessary notifications were made. 25 tons of soil were removed.
Detailed record list
Report Received Date
2015-08-27 00:00:00
Iyear
2015
Report Number
20150307
Supplemental Number
21175
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2015-07-28 11:45:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
0.48
Recovered Bbls
0.48
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-07-28 11:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-07-28 12:01:00
Restart Datetime
2015-07-28 14:39:00
On Site Datetime
2015-07-28 11:45:00
Nrc Rpt Datetime
2015-07-29 05:55:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Valve 34
Segment Name
Mn165xx
Onshore State Abbreviation
In
Onshore Postal Code
47303
Onshore City Name
Muncie
Onshore County Name
Delaware
Designated Location
Milepost/valve Station
Designated Name
280
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Wkm
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Valve Stem Packing
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
50
Est Cost Prop Damage
1000
Est Cost Emergency
8400
Est Cost Environmental
635
Est Cost Other
0
Prpty
10085
Accident Psig
235.5
Mop Psig
1411
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
386967
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The valve was not being operated at the time of the release and the release was caused by valve stem packing failure which the control center does not affect.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Unknown
Preparer Name
M***** E*****
Preparer Title
Districy Compliance Specalist
Preparer Email
M******@b******.com
Preparer Telephone
2197968230
Prepared Date
2016-02-26 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
6109044113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
Employee performing maintenance tasks had his air monitor alarmed with a high lel reading. The control center shutdown line 165 to isolate the section. A line probe was used down the side of the valve and it did not indicate any free product. Upon excavation product could be seen weeping from the valve stem. Packing was added to stop the leak and the contaminated soil was removed. All necessary notifications were made. 25 tons of soil were removed.
Report Received Date 2015-08-27 00:00:00
Iyear 2015
Report Number 20150307
Supplemental Number 21175
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2015-07-28 11:45:00
Location Latitude 40.279346 Google Maps OpenStreetMap
Location Longitude -85.363609 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 0.48
Recovered Bbls 0.48
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-07-28 11:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-07-28 12:01:00
Restart Datetime 2015-07-28 14:39:00
On Site Datetime 2015-07-28 11:45:00
Nrc Rpt Datetime 2015-07-29 05:55:00
Nrc Rpt Num 1124161 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Valve 34
Segment Name Mn165xx
Onshore State Abbreviation In
Onshore Postal Code 47303
Onshore City Name Muncie
Onshore County Name Delaware
Designated Location Milepost/valve Station
Designated Name 280
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Wkm
Installation Year Unknown
Manufactured Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details Valve Stem Packing
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 50
Est Cost Prop Damage 1000
Est Cost Emergency 8400
Est Cost Environmental 635
Est Cost Other 0
Prpty 10085
Accident Psig 235.5
Mop Psig 1411
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 386967
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The valve was not being operated at the time of the release and the release was caused by valve stem packing failure which the control center does not affect.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind Yes
Eq Additional Other Details Unknown
Preparer Name M***** E*****
Preparer Title Districy Compliance Specalist
Preparer Email M******@b******.com
Preparer Telephone 2197968230
Prepared Date 2016-02-26 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 6109044113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative Employee performing maintenance tasks had his air monitor alarmed with a high lel reading. The control center shutdown line 165 to isolate the section. A line probe was used down the side of the valve and it did not indicate any free product. Upon excavation product could be seen weeping from the valve stem. Packing was added to stop the leak and the contaminated soil was removed. All necessary notifications were made. 25 tons of soil were removed.

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