HL incident on 2015-07-22 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Natural Force Damage
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$207,262
Incident datetime
2015-07-22 13:25
Report number
Location
TX
Narrative
On july 22, 2015 at approximately 1:25 pm, a gauger discovered approximately 14 barrels of oil on the ground near the line 6a ultrasonic flow meter at the superior terminal. The gauger contacted the edmonton control center and line 6a was shutdown. The superior plm was dispatched to begin clean up and excavate to determine the leak source. It was discovered that the small diameter piping on the line 6 valve 6-ov-6c, which is on the suction side of the line 6 station, had failed. The two seat packing pipes had broken off at the point where they entered into the valve body. All six piping assemblies were schedule 80 and have been replaced with schedule 160. The fittings (elbow) have also been upgraded from a 2000 # rating to a 3000 # rating. Further investigation revealed that the release was due to frost heaving the small diameter piping assemblies. Approximately 380 cubic yards of contaminated soil have been hauled away to an approved landfill.
Detailed record list
Report Received Date
2015-08-20 00:00:00
Iyear
2015
Report Number
20150297
Supplemental Number
20681
Report Type
Original Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2015-07-22 13:25:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
13.9
Recovered Bbls
13.9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-07-22 13:25:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-07-22 13:30:00
Restart Datetime
2015-07-23 04:55:00
On Site Datetime
2015-07-22 13:25:00
Nrc Rpt Datetime
2015-07-22 14:37:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Line 6
Segment Name
6-Ov-6c
Onshore State Abbreviation
Wi
Onshore Postal Code
54880
Onshore City Name
Superior
Onshore County Name
Douglas
Designated Location
Milepost/valve Station
Designated Name
Superior Term
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
106
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2000
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
650
Est Cost Prop Damage
207262
Est Cost Emergency
26178
Est Cost Environmental
47750
Est Cost Other
0
Prpty
281840
Accident Psig
174
Mop Psig
684
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Temperature
Natural Force Type
Temperature
Temperature Subtype
Frost Heave
Nf Extreme Weather Ind
No
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Preparer Fax
715-394-1564
Prepared Date
2015-08-20 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Manager Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On july 22, 2015 at approximately 1:25 pm, a gauger discovered approximately 14 barrels of oil on the ground near the line 6a ultrasonic flow meter at the superior terminal. The gauger contacted the edmonton control center and line 6a was shutdown. The superior plm was dispatched to begin clean up and excavate to determine the leak source. It was discovered that the small diameter piping on the line 6 valve 6-ov-6c, which is on the suction side of the line 6 station, had failed. The two seat packing pipes had broken off at the point where they entered into the valve body. All six piping assemblies were schedule 80 and have been replaced with schedule 160. The fittings (elbow) have also been upgraded from a 2000 # rating to a 3000 # rating. Further investigation revealed that the release was due to frost heaving the small diameter piping assemblies. Approximately 380 cubic yards of contaminated soil have been hauled away to an approved landfill.
Report Received Date 2015-08-20 00:00:00
Iyear 2015
Report Number 20150297
Supplemental Number 20681
Report Type Original Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2015-07-22 13:25:00
Location Latitude 46.689722 Google Maps OpenStreetMap
Location Longitude -92.060556 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 13.9
Recovered Bbls 13.9
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-07-22 13:25:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-07-22 13:30:00
Restart Datetime 2015-07-23 04:55:00
On Site Datetime 2015-07-22 13:25:00
Nrc Rpt Datetime 2015-07-22 14:37:00
Nrc Rpt Num 1123571 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Line 6
Segment Name 6-Ov-6c
Onshore State Abbreviation Wi
Onshore Postal Code 54880
Onshore City Name Superior
Onshore County Name Douglas
Designated Location Milepost/valve Station
Designated Name Superior Term
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 106
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2000
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 650
Est Cost Prop Damage 207262
Est Cost Emergency 26178
Est Cost Environmental 47750
Est Cost Other 0
Prpty 281840
Accident Psig 174
Mop Psig 684
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Temperature
Natural Force Type Temperature
Temperature Subtype Frost Heave
Nf Extreme Weather Ind No
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Preparer Fax 715-394-1564
Prepared Date 2015-08-20 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Manager Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On july 22, 2015 at approximately 1:25 pm, a gauger discovered approximately 14 barrels of oil on the ground near the line 6a ultrasonic flow meter at the superior terminal. The gauger contacted the edmonton control center and line 6a was shutdown. The superior plm was dispatched to begin clean up and excavate to determine the leak source. It was discovered that the small diameter piping on the line 6 valve 6-ov-6c, which is on the suction side of the line 6 station, had failed. The two seat packing pipes had broken off at the point where they entered into the valve body. All six piping assemblies were schedule 80 and have been replaced with schedule 160. The fittings (elbow) have also been upgraded from a 2000 # rating to a 3000 # rating. Further investigation revealed that the release was due to frost heaving the small diameter piping assemblies. Approximately 380 cubic yards of contaminated soil have been hauled away to an approved landfill.

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