HL incident on 2015-07-22 — OK

Operator
Oneok Ngl Pipeline, Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$144,000
Incident datetime
2015-07-22 18:57
Report number
Location
OK
Narrative
At approximately 18:57 on 7/22/2015 a oneok employee conducting right of way clearing activities discovered dead vegetation on the oneok 14" wtlpg pipeline easement at mile post 52. Upon further investigation the employee determined a presence of hydrocarbons in the soil and contacted the pipeline supervisor. The pipeline supervisor along with the oneok pipeline control center immediately began reducing pressure on the pipeline and the 13 mile section of pipeline containing the suspected leak was isolated and removed from service. Nitrogen was used to purge the hydrocarbons from the isolated segment. Once purged, the suspected leak site was excavated and it was determined a weld, over a stud bolt, on a leak clamp installed in 2010 had a pin hole allowing hydrocarbons to be released. A 40.1' section of pipe containing the previously installed leak clamp was removed from the pipeline and new pre-tested pipe was installed. The pipeline was returned to service at 23:00 hrs. On july 25, 2015.
Detailed record list
Report Received Date
2015-08-19 00:00:00
Iyear
2015
Report Number
20150293
Supplemental Number
20676
Report Type
Original
Operator Id
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2015-07-22 18:57:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
5
Intentional Release Bbls
5
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-07-22 18:57:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-07-22 19:10:00
Restart Datetime
2015-07-25 03:20:00
On Site Datetime
2015-07-22 18:57:00
Nrc Rpt Datetime
2015-07-22 20:05:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Eastland To Weatherford 14"
Segment Name
20210
Onshore State Abbreviation
Tx
Onshore Postal Code
76472
Onshore City Name
Not Within A Municipality
Onshore County Name
Palo Pinto
Designated Location
Milepost/valve Station
Designated Name
Mp 52
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
53
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Tdw Leak Clamp
Installation Year
2010
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
135
Est Cost Prop Damage
144000
Est Cost Emergency
2500
Est Cost Environmental
3340
Est Cost Other
0
Prpty
149975
Accident Psig
550
Mop Psig
863
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
58080
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No controller actions had occurred prior to the release
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Pinhole In Weld On Stud Bolt Of Tdw Leak Clamp. Bolt On Clamp Was Welded To Pipeline Following Manufactures Instructions To Make A Permanent Repair. Original Repair Occurred In October Of 2010.
Eq Additional Other Ind
Yes
Eq Additional Other Details
Pinhole In Weld On Stud Bolt Of Tdw Leak Clamp.
Preparer Name
N*** J****
Preparer Title
Regulatory Compliance Coordinator
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2015-08-19 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Coordinator
Authorizer Email
N*********@o****.com
Narrative
At approximately 18:57 on 7/22/2015 a oneok employee conducting right of way clearing activities discovered dead vegetation on the oneok 14" wtlpg pipeline easement at mile post 52. Upon further investigation the employee determined a presence of hydrocarbons in the soil and contacted the pipeline supervisor. The pipeline supervisor along with the oneok pipeline control center immediately began reducing pressure on the pipeline and the 13 mile section of pipeline containing the suspected leak was isolated and removed from service. Nitrogen was used to purge the hydrocarbons from the isolated segment. Once purged, the suspected leak site was excavated and it was determined a weld, over a stud bolt, on a leak clamp installed in 2010 had a pin hole allowing hydrocarbons to be released. A 40.1' section of pipe containing the previously installed leak clamp was removed from the pipeline and new pre-tested pipe was installed. The pipeline was returned to service at 23:00 hrs. On july 25, 2015.
Report Received Date 2015-08-19 00:00:00
Iyear 2015
Report Number 20150293
Supplemental Number 20676
Report Type Original
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2015-07-22 18:57:00
Location Latitude 32.603333 Google Maps OpenStreetMap
Location Longitude -98.114722 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 5
Intentional Release Bbls 5
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-07-22 18:57:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-07-22 19:10:00
Restart Datetime 2015-07-25 03:20:00
On Site Datetime 2015-07-22 18:57:00
Nrc Rpt Datetime 2015-07-22 20:05:00
Nrc Rpt Num 1123595 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Eastland To Weatherford 14"
Segment Name 20210
Onshore State Abbreviation Tx
Onshore Postal Code 76472
Onshore City Name Not Within A Municipality
Onshore County Name Palo Pinto
Designated Location Milepost/valve Station
Designated Name Mp 52
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 53
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Tdw Leak Clamp
Installation Year 2010
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 135
Est Cost Prop Damage 144000
Est Cost Emergency 2500
Est Cost Environmental 3340
Est Cost Other 0
Prpty 149975
Accident Psig 550
Mop Psig 863
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 58080
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No controller actions had occurred prior to the release
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Pinhole In Weld On Stud Bolt Of Tdw Leak Clamp. Bolt On Clamp Was Welded To Pipeline Following Manufactures Instructions To Make A Permanent Repair. Original Repair Occurred In October Of 2010.
Eq Additional Other Ind Yes
Eq Additional Other Details Pinhole In Weld On Stud Bolt Of Tdw Leak Clamp.
Preparer Name N*** J****
Preparer Title Regulatory Compliance Coordinator
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2933
Prepared Date 2015-08-19 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Regulatory Compliance Coordinator
Authorizer Email N*********@o****.com
Narrative At approximately 18:57 on 7/22/2015 a oneok employee conducting right of way clearing activities discovered dead vegetation on the oneok 14" wtlpg pipeline easement at mile post 52. Upon further investigation the employee determined a presence of hydrocarbons in the soil and contacted the pipeline supervisor. The pipeline supervisor along with the oneok pipeline control center immediately began reducing pressure on the pipeline and the 13 mile section of pipeline containing the suspected leak was isolated and removed from service. Nitrogen was used to purge the hydrocarbons from the isolated segment. Once purged, the suspected leak site was excavated and it was determined a weld, over a stud bolt, on a leak clamp installed in 2010 had a pin hole allowing hydrocarbons to be released. A 40.1' section of pipe containing the previously installed leak clamp was removed from the pipeline and new pre-tested pipe was installed. The pipeline was returned to service at 23:00 hrs. On july 25, 2015.

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