HL incident on 2015-07-27 — PA

Operator
Buckeye Partners, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000
Incident datetime
2015-07-27 06:00
Report number
Location
PA
Narrative
On the morning of july 27, 2015 a local booth controller, detected the smell of gasoline emitting from the manifold area. A subsequent check of the station revealed that gasoline was weeping from the incoming valve to tank 19. The valve was close and the weeping stopped. The approximately 10 gallons of product was siphoned off using a vac truck. The valve packing was replaced, closely monitored and the valve returned to service. The total costs associated with this release are about $1,000.00. There is no pending remediation planned.
Detailed record list
Report Received Date
2015-08-19 00:00:00
Iyear
2015
Report Number
20150292
Supplemental Number
21072
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2015-07-27 06:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.23
Recovered Bbls
0.23
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-07-27 06:00:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Valve Was Closed To Stop The Weeping Of Product
On Site Datetime
2015-07-27 06:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Booth Station
Segment Name
Bh
Onshore State Abbreviation
Pa
Onshore Postal Code
19061
Onshore City Name
Boothwyn
Onshore County Name
Delaware
Designated Location
Survey Station No.
Designated Name
Bh Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Tank Type
Atmospheric
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
1000
Est Cost Emergency
100
Est Cost Environmental
0
Est Cost Other
0
Prpty
1100
Accident Psig
23.3
Mop Psig
642
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak was too small to be detected by mechanical methods
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Check Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Excessive Weeping Of Valve Packing
Preparer Name
H*** S******
Preparer Title
Sr. Compliance Specialist
Preparer Email
H*******@b******.com
Preparer Telephone
610-904-4916
Prepared Date
2016-01-21 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
On the morning of july 27, 2015 a local booth controller, detected the smell of gasoline emitting from the manifold area. A subsequent check of the station revealed that gasoline was weeping from the incoming valve to tank 19. The valve was close and the weeping stopped. The approximately 10 gallons of product was siphoned off using a vac truck. The valve packing was replaced, closely monitored and the valve returned to service. The total costs associated with this release are about $1,000.00. There is no pending remediation planned.
Report Received Date 2015-08-19 00:00:00
Iyear 2015
Report Number 20150292
Supplemental Number 21072
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2015-07-27 06:00:00
Location Latitude 39.846349 Google Maps OpenStreetMap
Location Longitude -75.459406 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.23
Recovered Bbls 0.23
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-07-27 06:00:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Valve Was Closed To Stop The Weeping Of Product
On Site Datetime 2015-07-27 06:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Booth Station
Segment Name Bh
Onshore State Abbreviation Pa
Onshore Postal Code 19061
Onshore City Name Boothwyn
Onshore County Name Delaware
Designated Location Survey Station No.
Designated Name Bh Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Tank Type Atmospheric
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 1000
Est Cost Emergency 100
Est Cost Environmental 0
Est Cost Other 0
Prpty 1100
Accident Psig 23.3
Mop Psig 642
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak was too small to be detected by mechanical methods
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Check Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Excessive Weeping Of Valve Packing
Preparer Name H*** S******
Preparer Title Sr. Compliance Specialist
Preparer Email H*******@b******.com
Preparer Telephone 610-904-4916
Prepared Date 2016-01-21 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative On the morning of july 27, 2015 a local booth controller, detected the smell of gasoline emitting from the manifold area. A subsequent check of the station revealed that gasoline was weeping from the incoming valve to tank 19. The valve was close and the weeping stopped. The approximately 10 gallons of product was siphoned off using a vac truck. The valve packing was replaced, closely monitored and the valve returned to service. The total costs associated with this release are about $1,000.00. There is no pending remediation planned.

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