HL incident on 2015-07-20 — TX

Operator
Enbridge Pipelines (Toledo) Inc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$300
Incident datetime
2015-07-20 12:50
Report number
Location
TX
Narrative
On july 20, 2015 at 12:50 pm while performing rounds at the oregon metering facility, the station electrical technician discovered a release from a meter run isolation valve (151-v-113) in the meter skid containment area. Upon immediate visual inspection, 100 gallons of product was estimated to have originated from the failed 1/2" block and bleed tubing attached to the body of the valve. After dimensions of impacted soil were taken by a pipeline maintenance supervisor, a revised estimate of 252 gallons was calculated. The estimated cost of cleanup was expected to exceed the reporting threshold of $50,000, so the nrc was notified (nrc report # 1123318). The meter run was isolated to prevent further release of product and the station technician replaced the body bleed failed tubing. A field examination of the failed tubing showed localized pitting at the manufactured bend. The pipeline maintenance crew arrived on site and executed cleanup. Approximately 40 yards of contaminated soil was removed and disposed of at an approved site. The failed tubing has been sent in for a failure analysis.
Detailed record list
Report Received Date
2015-08-18 00:00:00
Iyear
2015
Report Number
20150291
Supplemental Number
20674
Report Type
Original Final
Operator Id
Name
Enbridge Pipelines (Toledo) Inc
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2015-07-20 12:50:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
6.02
Recovered Bbls
6.02
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-07-20 12:50:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-07-20 12:50:00
Restart Datetime
2015-07-20 17:25:00
On Site Datetime
2015-07-20 12:50:00
Nrc Rpt Datetime
2015-07-20 13:58:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Oregon Metering Facility
Segment Name
151-V-113
Onshore State Abbreviation
Oh
Onshore Postal Code
43616
Onshore City Name
Oregon
Onshore County Name
Lucas
Designated Location
Milepost/valve Station
Designated Name
88.11
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
1999
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
242
Est Cost Prop Damage
300
Est Cost Emergency
60642
Est Cost Environmental
25780
Est Cost Other
0
Prpty
86964
Accident Psig
239
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No control center involvement as it was a tubing failure on the block and bleed.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Field Exam Basis Ind
Yes
Int Other Loc Ind
Yes
Corrosion Location Details
Manufactured Bend
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Preparer Fax
715-394-1564
Prepared Date
2015-08-18 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
715-395-3619
Authorizer Title
Manager Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On july 20, 2015 at 12:50 pm while performing rounds at the oregon metering facility, the station electrical technician discovered a release from a meter run isolation valve (151-v-113) in the meter skid containment area. Upon immediate visual inspection, 100 gallons of product was estimated to have originated from the failed 1/2" block and bleed tubing attached to the body of the valve. After dimensions of impacted soil were taken by a pipeline maintenance supervisor, a revised estimate of 252 gallons was calculated. The estimated cost of cleanup was expected to exceed the reporting threshold of $50,000, so the nrc was notified (nrc report # 1123318). The meter run was isolated to prevent further release of product and the station technician replaced the body bleed failed tubing. A field examination of the failed tubing showed localized pitting at the manufactured bend. The pipeline maintenance crew arrived on site and executed cleanup. Approximately 40 yards of contaminated soil was removed and disposed of at an approved site. The failed tubing has been sent in for a failure analysis.
Report Received Date 2015-08-18 00:00:00
Iyear 2015
Report Number 20150291
Supplemental Number 20674
Report Type Original Final
Operator Id 31448 PHMSA Enforcement
Name Enbridge Pipelines (Toledo) Inc
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2015-07-20 12:50:00
Location Latitude 41.67284 Google Maps OpenStreetMap
Location Longitude -83.45352 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 6.02
Recovered Bbls 6.02
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-07-20 12:50:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-07-20 12:50:00
Restart Datetime 2015-07-20 17:25:00
On Site Datetime 2015-07-20 12:50:00
Nrc Rpt Datetime 2015-07-20 13:58:00
Nrc Rpt Num 1123318 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Oregon Metering Facility
Segment Name 151-V-113
Onshore State Abbreviation Oh
Onshore Postal Code 43616
Onshore City Name Oregon
Onshore County Name Lucas
Designated Location Milepost/valve Station
Designated Name 88.11
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year 1999
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 242
Est Cost Prop Damage 300
Est Cost Emergency 60642
Est Cost Environmental 25780
Est Cost Other 0
Prpty 86964
Accident Psig 239
Mop Psig 720
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No control center involvement as it was a tubing failure on the block and bleed.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Water Acid Ind Yes
Int Field Exam Basis Ind Yes
Int Other Loc Ind Yes
Corrosion Location Details Manufactured Bend
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Preparer Fax 715-394-1564
Prepared Date 2015-08-18 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 715-395-3619
Authorizer Title Manager Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On july 20, 2015 at 12:50 pm while performing rounds at the oregon metering facility, the station electrical technician discovered a release from a meter run isolation valve (151-v-113) in the meter skid containment area. Upon immediate visual inspection, 100 gallons of product was estimated to have originated from the failed 1/2" block and bleed tubing attached to the body of the valve. After dimensions of impacted soil were taken by a pipeline maintenance supervisor, a revised estimate of 252 gallons was calculated. The estimated cost of cleanup was expected to exceed the reporting threshold of $50,000, so the nrc was notified (nrc report # 1123318). The meter run was isolated to prevent further release of product and the station technician replaced the body bleed failed tubing. A field examination of the failed tubing showed localized pitting at the manufactured bend. The pipeline maintenance crew arrived on site and executed cleanup. Approximately 40 yards of contaminated soil was removed and disposed of at an approved site. The failed tubing has been sent in for a failure analysis.

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