HL incident on 2015-07-24 — GA

Operator
Colonial Pipeline Co
Cause
Excavation Issue
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2015-07-24 14:18
Report number
Location
GA
Narrative
On 7/24/2015 at 14:15 a contract crew damaged a buried tubing line during excavation near the line 02 unit 5 discharge valve inside houston station. The 3/8 inch armor-coated tubing was connected to unit 5 case pressure instrumentation. The tubing was struck by a mini excavator and pulled apart, releasing 80 gallons of diesel fuel before it was isolated. Internal notifications were made and a technician and contractor crew working at the site immediately started clean up and repair activities. Temporary repairs were completed by 15:00 and the line was restarted at 15:20. Final cleanup efforts were completed by 18:50. All released product was contained on company property in the immediate area. No immediate state, local or federal agency notifications were required due to the volume released and that it was contained on company property. A post-accident drug and alcohol test was conducted on the contract operator of the mini excavator.
Detailed record list
Report Received Date
2015-08-13 00:00:00
Iyear
2015
Report Number
20150286
Supplemental Number
20902
Report Type
Supplemental Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1000 Lake St.
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009
Local Datetime
2015-07-24 14:15:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
1.9
Recovered Bbls
1.9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2015-07-24 14:18:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-07-24 14:18:00
Restart Datetime
2015-07-24 15:20:00
On Site Datetime
2015-07-24 14:18:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Houston Station
Segment Name
Line 02 Unit 5 Case Pressure Switch Tubing
Onshore State Abbreviation
Tx
Onshore Postal Code
77506
Onshore City Name
Pasadena
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
120
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
10
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
1985
Material Involved
Material Other Than Carbon Steel
Material Details
Copper
Release Type
Other
Release Type Details
Excavation Damage To Tubing Line For Instrumentation
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
240
Est Cost Prop Damage
0
Est Cost Emergency
4760
Est Cost Environmental
0
Est Cost Other
0
Prpty
5000
Accident Psig
170
Mop Psig
960
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Release resulted from damage caused by contractor excavation activities. No controller or control room issues contributed to the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
1
Num Contractors Failed
0
Cause
Excavation Damage
Cause Details
Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type
Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt
Yes
Pipeline Easement Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Liquid Pipeline
One Call Notified Ind
Yes
One Call Ticket Num
1570565889
One Call Center Name
Texas 811
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
1
Root Cause Category
Excavation Issue
Root Cause Type
Improper Excavation Practice Not Listed Above
Preparer Name
K**** M****
Preparer Title
Compliance Coordinator
Preparer Email
K*****@c******.com
Preparer Telephone
601-765-9168
Preparer Fax
770-754-8489
Prepared Date
2015-11-12 00:00:00
Authorizer Name
D*** L*****
Authorizer Telephone
678-762-2872
Authorizer Title
Phmsa Compliance Manager
Authorizer Email
D******@c******.com
Narrative
On 7/24/2015 at 14:15 a contract crew damaged a buried tubing line during excavation near the line 02 unit 5 discharge valve inside houston station. The 3/8 inch armor-coated tubing was connected to unit 5 case pressure instrumentation. The tubing was struck by a mini excavator and pulled apart, releasing 80 gallons of diesel fuel before it was isolated. Internal notifications were made and a technician and contractor crew working at the site immediately started clean up and repair activities. Temporary repairs were completed by 15:00 and the line was restarted at 15:20. Final cleanup efforts were completed by 18:50. All released product was contained on company property in the immediate area. No immediate state, local or federal agency notifications were required due to the volume released and that it was contained on company property. A post-accident drug and alcohol test was conducted on the contract operator of the mini excavator.
Report Received Date 2015-08-13 00:00:00
Iyear 2015
Report Number 20150286
Supplemental Number 20902
Report Type Supplemental Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1000 Lake St.
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009
Local Datetime 2015-07-24 14:15:00
Location Latitude 29.71897 Google Maps OpenStreetMap
Location Longitude -95.1793 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 1.9
Recovered Bbls 1.9
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2015-07-24 14:18:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-07-24 14:18:00
Restart Datetime 2015-07-24 15:20:00
On Site Datetime 2015-07-24 14:18:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Houston Station
Segment Name Line 02 Unit 5 Case Pressure Switch Tubing
Onshore State Abbreviation Tx
Onshore Postal Code 77506
Onshore City Name Pasadena
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 120
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 10
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year 1985
Material Involved Material Other Than Carbon Steel
Material Details Copper
Release Type Other
Release Type Details Excavation Damage To Tubing Line For Instrumentation
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 240
Est Cost Prop Damage 0
Est Cost Emergency 4760
Est Cost Environmental 0
Est Cost Other 0
Prpty 5000
Accident Psig 170
Mop Psig 960
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Release resulted from damage caused by contractor excavation activities. No controller or control room issues contributed to the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind Yes
Num Contractors Tested 1
Num Contractors Failed 0
Cause Excavation Damage
Cause Details Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt Yes
Pipeline Easement Row Ind Yes
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Liquid Pipeline
One Call Notified Ind Yes
One Call Ticket Num 1570565889
One Call Center Name Texas 811
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 1
Root Cause Category Excavation Issue
Root Cause Type Improper Excavation Practice Not Listed Above
Preparer Name K**** M****
Preparer Title Compliance Coordinator
Preparer Email K*****@c******.com
Preparer Telephone 601-765-9168
Preparer Fax 770-754-8489
Prepared Date 2015-11-12 00:00:00
Authorizer Name D*** L*****
Authorizer Telephone 678-762-2872
Authorizer Title Phmsa Compliance Manager
Authorizer Email D******@c******.com
Narrative On 7/24/2015 at 14:15 a contract crew damaged a buried tubing line during excavation near the line 02 unit 5 discharge valve inside houston station. The 3/8 inch armor-coated tubing was connected to unit 5 case pressure instrumentation. The tubing was struck by a mini excavator and pulled apart, releasing 80 gallons of diesel fuel before it was isolated. Internal notifications were made and a technician and contractor crew working at the site immediately started clean up and repair activities. Temporary repairs were completed by 15:00 and the line was restarted at 15:20. Final cleanup efforts were completed by 18:50. All released product was contained on company property in the immediate area. No immediate state, local or federal agency notifications were required due to the volume released and that it was contained on company property. A post-accident drug and alcohol test was conducted on the contract operator of the mini excavator.

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