HL incident on 2015-07-15 — TX

Operator
Ccps Transportation, Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2015-07-15 08:34
Report number
Location
TX
Narrative
On july 1, 2015 at 8:34 am, a maintenance technician discovered a stem seal leak at key station on line 55 on the station by-pass valve (ky-55-bv-1). Initially, it was estimated that approximately 10-15 gallons of crude oil was released onto the ground. The valve stem seal was re-packed to stop the leak and no further repairs were needed. During clean up, the estimated release amount changed to 42 gallons due to additional oil found in the sand under the gravel. The estimated cost then rose to the nrc reporting threshold. Line 55 was not shut down during this incident as it was already shut down for scheduled maintenance on july 14, 2015 at 6:00 am. Contractors completed the cleanup work during this timeframe and the line was returned to service as scheduled on july 15, 2015 at 10:47 am.
Detailed record list
Report Received Date
2015-08-10 00:00:00
Iyear
2015
Report Number
20150280
Supplemental Number
20657
Report Type
Original Final
Operator Id
Name
Ccps Transportation, Llc
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2015-07-15 08:34:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-07-15 08:34:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Occurred During A Scheduled Shutdown
On Site Datetime
2015-07-15 08:34:00
Nrc Rpt Datetime
2015-07-15 18:32:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Key Station
Segment Name
Ky-55-Bv-1
Onshore State Abbreviation
Mo
Onshore Postal Code
65281
Onshore City Name
Salisbury
Onshore County Name
Chariton
Designated Location
Milepost/valve Station
Designated Name
5565
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
1951
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
100
Est Cost Emergency
20000
Est Cost Environmental
30000
Est Cost Other
0
Prpty
50120
Accident Psig
325
Mop Psig
1054
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Lack of control center involvement
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Stem Seal
Eq Additional Other Ind
Yes
Eq Additional Other Details
Normal Wear And Tear
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
7153953620
Preparer Fax
7153941564
Prepared Date
2015-08-10 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
7153953619
Authorizer Title
Manager Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On july 1, 2015 at 8:34 am, a maintenance technician discovered a stem seal leak at key station on line 55 on the station by-pass valve (ky-55-bv-1). Initially, it was estimated that approximately 10-15 gallons of crude oil was released onto the ground. The valve stem seal was re-packed to stop the leak and no further repairs were needed. During clean up, the estimated release amount changed to 42 gallons due to additional oil found in the sand under the gravel. The estimated cost then rose to the nrc reporting threshold. Line 55 was not shut down during this incident as it was already shut down for scheduled maintenance on july 14, 2015 at 6:00 am. Contractors completed the cleanup work during this timeframe and the line was returned to service as scheduled on july 15, 2015 at 10:47 am.
Report Received Date 2015-08-10 00:00:00
Iyear 2015
Report Number 20150280
Supplemental Number 20657
Report Type Original Final
Operator Id 32080 PHMSA Enforcement
Name Ccps Transportation, Llc
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2015-07-15 08:34:00
Location Latitude 39.411914 Google Maps OpenStreetMap
Location Longitude -92.842889 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-07-15 08:34:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Occurred During A Scheduled Shutdown
On Site Datetime 2015-07-15 08:34:00
Nrc Rpt Datetime 2015-07-15 18:32:00
Nrc Rpt Num 1122905 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Key Station
Segment Name Ky-55-Bv-1
Onshore State Abbreviation Mo
Onshore Postal Code 65281
Onshore City Name Salisbury
Onshore County Name Chariton
Designated Location Milepost/valve Station
Designated Name 5565
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 1951
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 20
Est Cost Prop Damage 100
Est Cost Emergency 20000
Est Cost Environmental 30000
Est Cost Other 0
Prpty 50120
Accident Psig 325
Mop Psig 1054
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Lack of control center involvement
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Stem Seal
Eq Additional Other Ind Yes
Eq Additional Other Details Normal Wear And Tear
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 7153953620
Preparer Fax 7153941564
Prepared Date 2015-08-10 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 7153953619
Authorizer Title Manager Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On july 1, 2015 at 8:34 am, a maintenance technician discovered a stem seal leak at key station on line 55 on the station by-pass valve (ky-55-bv-1). Initially, it was estimated that approximately 10-15 gallons of crude oil was released onto the ground. The valve stem seal was re-packed to stop the leak and no further repairs were needed. During clean up, the estimated release amount changed to 42 gallons due to additional oil found in the sand under the gravel. The estimated cost then rose to the nrc reporting threshold. Line 55 was not shut down during this incident as it was already shut down for scheduled maintenance on july 14, 2015 at 6:00 am. Contractors completed the cleanup work during this timeframe and the line was returned to service as scheduled on july 15, 2015 at 10:47 am.

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