HL incident on 2015-07-07 — TX

Operator
West Texas Gulf Pipeline Co
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$15,000
Incident datetime
2015-07-07 13:55
Report number
Location
TX
Narrative
At ranger station, an inline strainer failed resulting in debris hitting the flow switch probes in the suction piping to the pump. The damage to the flow switch probes allowed oil to enter the flow switch instrumentation and approximately 10 gallons was released from the conduit. The remaining damaged inline strainer was removed and a new flow switch and flange gasket were installed. The contaminated soil was removed from the immediate area and remediated onsite.
Detailed record list
Report Received Date
2015-08-05 00:00:00
Iyear
2015
Report Number
20150274
Supplemental Number
20647
Report Type
Original Final
Operator Id
Name
West Texas Gulf Pipeline Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-07-07 13:55:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.24
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2015-07-07 13:55:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Piping Isolated Via Valve Realignment.
On Site Datetime
2015-07-07 15:45:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Ranger Station
Segment Name
Ranger Station Manifold Piping
Onshore State Abbreviation
Tx
Onshore Postal Code
76470
Onshore City Name
Ranger
Onshore County Name
Eastland
Designated Location
Milepost/valve Station
Designated Name
Mp 131.6
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Instrumentation
Installation Year
2014
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel Flow Switch & Conduit
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
250
Est Cost Prop Damage
15000
Est Cost Emergency
1000
Est Cost Environmental
1000
Est Cost Other
0
Prpty
17250
Accident Psig
75
Mop Psig
750
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Failure Of A Flow Switch Due To Debris From A Damaged Inline Strainer That Impacted The Flow Switch Probes Inside The Piping.
Eq Additional Other Ind
Yes
Eq Additional Other Details
Failed Inline Strainer Parts Impacted Flow Switch Probes Inside The Piping
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2015-08-05 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
At ranger station, an inline strainer failed resulting in debris hitting the flow switch probes in the suction piping to the pump. The damage to the flow switch probes allowed oil to enter the flow switch instrumentation and approximately 10 gallons was released from the conduit. The remaining damaged inline strainer was removed and a new flow switch and flange gasket were installed. The contaminated soil was removed from the immediate area and remediated onsite.
Report Received Date 2015-08-05 00:00:00
Iyear 2015
Report Number 20150274
Supplemental Number 20647
Report Type Original Final
Operator Id 22442 PHMSA Enforcement
Name West Texas Gulf Pipeline Co
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-07-07 13:55:00
Location Latitude 32.49804 Google Maps OpenStreetMap
Location Longitude -98.63654 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.24
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2015-07-07 13:55:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Piping Isolated Via Valve Realignment.
On Site Datetime 2015-07-07 15:45:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Ranger Station
Segment Name Ranger Station Manifold Piping
Onshore State Abbreviation Tx
Onshore Postal Code 76470
Onshore City Name Ranger
Onshore County Name Eastland
Designated Location Milepost/valve Station
Designated Name Mp 131.6
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Instrumentation
Installation Year 2014
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel Flow Switch & Conduit
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 250
Est Cost Prop Damage 15000
Est Cost Emergency 1000
Est Cost Environmental 1000
Est Cost Other 0
Prpty 17250
Accident Psig 75
Mop Psig 750
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Failure Of A Flow Switch Due To Debris From A Damaged Inline Strainer That Impacted The Flow Switch Probes Inside The Piping.
Eq Additional Other Ind Yes
Eq Additional Other Details Failed Inline Strainer Parts Impacted Flow Switch Probes Inside The Piping
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2015-08-05 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative At ranger station, an inline strainer failed resulting in debris hitting the flow switch probes in the suction piping to the pump. The damage to the flow switch probes allowed oil to enter the flow switch instrumentation and approximately 10 gallons was released from the conduit. The remaining damaged inline strainer was removed and a new flow switch and flange gasket were installed. The contaminated soil was removed from the immediate area and remediated onsite.

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