HL incident on 2015-07-02 — TX

Operator
Rose Rock Midstream L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$8,000
Incident datetime
2015-07-02 10:56
Report number
Location
TX
Narrative
A small area of ground was found to be discolored by aerial patrol. The pipeline was shut in and the leak area was excavated finding a small pinhole in the pipe. Upon inspection of the pipe, our corrosion tech collected a sample of water to check for bacteria and corrosion inhibitor. A full encirclement sleeve was welded on the pipeline for the pipeline repair. Internal corrosion created a pinhole leak. The leak was very small and most likely surfaced due to recent rain. There was minimal remediation required. Failure was attributed to not performing regular cleaning pigs to ensure the biocide that was being injected into the pipeline monthly had surface contact with corrosion causing bacterial. There is low flow of oil in this pipeline which limits running cleaning pigs through the pipeline. An ili is scheduled to be performed on this pipeline in 2016.
Detailed record list
Report Received Date
2015-07-31 00:00:00
Iyear
2015
Report Number
20150273
Supplemental Number
21138
Report Type
Supplemental Final
Operator Id
Name
Rose Rock Midstream L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-07-02 10:56:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.5
Recovered Bbls
0.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Aerial Patrol Found Small Area Of Ground Discoloration
Incident Identified Datetime
2015-07-02 10:56:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-07-02 11:35:00
Restart Datetime
2015-07-03 11:00:00
On Site Datetime
2015-07-02 11:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Cunningham To Arlington Jct. 12"
Segment Name
Cunningham To Arlington Jct. 12"
Onshore State Abbreviation
Ks
Onshore Postal Code
67068
Onshore City Name
Not Within A Municipality
Onshore County Name
Kingman
Designated Location
Milepost/valve Station
Designated Name
2
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
65
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12
Pipe Wall Thickness
0.375
Pipe Smys
24000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1934
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
8000
Est Cost Emergency
2500
Est Cost Environmental
2000
Est Cost Other
0
Prpty
12520
Accident Psig
50
Mop Psig
600
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
95040
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak was internal corrosion and was a seep not detected by controller.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Other Corrosion Ind
Yes
Int Corrosion Type Details
Sample Sent To Baker Hughes For Analysis
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
No
Corrosion Coupons
Yes
Collected Data Ind
Yes
Geometry Recent Year
2010
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2012
Hydrtst Most Rcnt Pressure
780
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
R**** S******
Preparer Title
District Manager
Preparer Email
R*******@s***********.com
Preparer Telephone
620-474-6190
Preparer Fax
620-239-5388
Prepared Date
2016-02-18 00:00:00
Authorizer Name
T*** A*******
Authorizer Telephone
918-524-8109
Authorizer Title
Dot Compliance Manager
Authorizer Email
T********@s***********.com
Narrative
A small area of ground was found to be discolored by aerial patrol. The pipeline was shut in and the leak area was excavated finding a small pinhole in the pipe. Upon inspection of the pipe, our corrosion tech collected a sample of water to check for bacteria and corrosion inhibitor. A full encirclement sleeve was welded on the pipeline for the pipeline repair. Internal corrosion created a pinhole leak. The leak was very small and most likely surfaced due to recent rain. There was minimal remediation required. Failure was attributed to not performing regular cleaning pigs to ensure the biocide that was being injected into the pipeline monthly had surface contact with corrosion causing bacterial. There is low flow of oil in this pipeline which limits running cleaning pigs through the pipeline. An ili is scheduled to be performed on this pipeline in 2016.
Report Received Date 2015-07-31 00:00:00
Iyear 2015
Report Number 20150273
Supplemental Number 21138
Report Type Supplemental Final
Operator Id 31476 PHMSA Enforcement
Name Rose Rock Midstream L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-07-02 10:56:00
Location Latitude 37.68779 Google Maps OpenStreetMap
Location Longitude -98.40713 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.5
Recovered Bbls 0.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Aerial Patrol Found Small Area Of Ground Discoloration
Incident Identified Datetime 2015-07-02 10:56:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-07-02 11:35:00
Restart Datetime 2015-07-03 11:00:00
On Site Datetime 2015-07-02 11:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Cunningham To Arlington Jct. 12"
Segment Name Cunningham To Arlington Jct. 12"
Onshore State Abbreviation Ks
Onshore Postal Code 67068
Onshore City Name Not Within A Municipality
Onshore County Name Kingman
Designated Location Milepost/valve Station
Designated Name 2
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 65
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 12
Pipe Wall Thickness 0.375
Pipe Smys 24000
Pipe Specification Api 5l
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1934
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 20
Est Cost Prop Damage 8000
Est Cost Emergency 2500
Est Cost Environmental 2000
Est Cost Other 0
Prpty 12520
Accident Psig 50
Mop Psig 600
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 95040
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The leak was internal corrosion and was a seep not detected by controller.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Other Corrosion Ind Yes
Int Corrosion Type Details Sample Sent To Baker Hughes For Analysis
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering No
Corrosion Coupons Yes
Collected Data Ind Yes
Geometry Recent Year 2010
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2012
Hydrtst Most Rcnt Pressure 780
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name R**** S******
Preparer Title District Manager
Preparer Email R*******@s***********.com
Preparer Telephone 620-474-6190
Preparer Fax 620-239-5388
Prepared Date 2016-02-18 00:00:00
Authorizer Name T*** A*******
Authorizer Telephone 918-524-8109
Authorizer Title Dot Compliance Manager
Authorizer Email T********@s***********.com
Narrative A small area of ground was found to be discolored by aerial patrol. The pipeline was shut in and the leak area was excavated finding a small pinhole in the pipe. Upon inspection of the pipe, our corrosion tech collected a sample of water to check for bacteria and corrosion inhibitor. A full encirclement sleeve was welded on the pipeline for the pipeline repair. Internal corrosion created a pinhole leak. The leak was very small and most likely surfaced due to recent rain. There was minimal remediation required. Failure was attributed to not performing regular cleaning pigs to ensure the biocide that was being injected into the pipeline monthly had surface contact with corrosion causing bacterial. There is low flow of oil in this pipeline which limits running cleaning pigs through the pipeline. An ili is scheduled to be performed on this pipeline in 2016.

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