HL incident on 2015-07-06 — GA

Operator
Colonial Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$3,000
Incident datetime
2015-07-06 08:00
Report number
Location
GA
Narrative
On july 6, 2015 at approximately 08:00 am, a senior operator was making rounds and noticed sheen of product inside the sting water tank access well. He notified the operations manager and lead operator of his finding. The oil water separator (ows) and sting water tank were isolated. Both the sting water tank and ows were temporarily locked out of service until repairs were complete. The sheen was collected in absorbents and the water was vacuumed up for disposal at approved recycling facility. Recovered product was less than six gallons. After further investigation by projects and environmental specialist, it was determined that the containment around the ows was not completely sealed. Although it is unlikely that the sting water breached the containment area, the determination was made to report this as potentially impacting the environment. On 7/13/15,courtesy notificationswere was made to virginia state corp commission which works on behalf of PHMSA in virginia. No other agencies were notified since it was less than 25 gallons. 3/18/2016: I was determined that the gasket on the tank valve had failed. The gasket was replaced on the tank valve; all repairs are complete.
Detailed record list
Report Received Date
2015-07-29 00:00:00
Iyear
2015
Report Number
20150269
Supplemental Number
21251
Report Type
Supplemental Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1000 Lake St.
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009
Local Datetime
2015-07-06 08:00:00
Location Latitude
Location Longitude
-78.23750439
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
0.12
Recovered Bbls
0.12
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-07-06 08:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
There Was No Impact On Operation Of The Pipeline
On Site Datetime
2015-07-06 08:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Mitchell Junction
Segment Name
Line 03/04
Onshore State Abbreviation
Va
Onshore Postal Code
23038
Onshore City Name
Columbia
Onshore County Name
Cumberland
Designated Location
Survey Station No.
Designated Name
Loc 0946
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
In Underground Enclosed Space (E.g. Vault)
Depth Of Cover
1
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
1997
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
15
Est Cost Prop Damage
3000
Est Cost Emergency
30000
Est Cost Environmental
0
Est Cost Other
1000
Est Cost Other Details
Technicians Time To Replace 3 Gaskets
Prpty
34015
Accident Psig
0
Mop Psig
0
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This area of the tank farm is not monitored by alpharetta control center.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Ief Addl Misalignment Ind
Yes
Preparer Name
A**** S****
Preparer Title
Compliance Coordinator
Preparer Email
A******@c******.com
Preparer Telephone
410 970 2157
Preparer Fax
770 754 8036
Prepared Date
2016-03-18 00:00:00
Authorizer Name
D*** L*****
Authorizer Telephone
678 762 2872
Authorizer Title
Manager Phmsa Regulatory Compliance
Authorizer Email
D******@c******.com
Narrative
On july 6, 2015 at approximately 08:00 am, a senior operator was making rounds and noticed sheen of product inside the sting water tank access well. He notified the operations manager and lead operator of his finding. The oil water separator (ows) and sting water tank were isolated. Both the sting water tank and ows were temporarily locked out of service until repairs were complete. The sheen was collected in absorbents and the water was vacuumed up for disposal at approved recycling facility. Recovered product was less than six gallons. After further investigation by projects and environmental specialist, it was determined that the containment around the ows was not completely sealed. Although it is unlikely that the sting water breached the containment area, the determination was made to report this as potentially impacting the environment. On 7/13/15,courtesy notificationswere was made to virginia state corp commission which works on behalf of PHMSA in virginia. No other agencies were notified since it was less than 25 gallons. 3/18/2016: I was determined that the gasket on the tank valve had failed. The gasket was replaced on the tank valve; all repairs are complete.
Report Received Date 2015-07-29 00:00:00
Iyear 2015
Report Number 20150269
Supplemental Number 21251
Report Type Supplemental Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1000 Lake St.
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009
Local Datetime 2015-07-06 08:00:00
Location Latitude 37.66330708 Google Maps OpenStreetMap
Location Longitude -78.23750439 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 0.12
Recovered Bbls 0.12
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-07-06 08:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain There Was No Impact On Operation Of The Pipeline
On Site Datetime 2015-07-06 08:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Mitchell Junction
Segment Name Line 03/04
Onshore State Abbreviation Va
Onshore Postal Code 23038
Onshore City Name Columbia
Onshore County Name Cumberland
Designated Location Survey Station No.
Designated Name Loc 0946
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype In Underground Enclosed Space (E.g. Vault)
Depth Of Cover 1
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 1997
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 15
Est Cost Prop Damage 3000
Est Cost Emergency 30000
Est Cost Environmental 0
Est Cost Other 1000
Est Cost Other Details Technicians Time To Replace 3 Gaskets
Prpty 34015
Accident Psig 0
Mop Psig 0
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This area of the tank farm is not monitored by alpharetta control center.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Ief Addl Misalignment Ind Yes
Preparer Name A**** S****
Preparer Title Compliance Coordinator
Preparer Email A******@c******.com
Preparer Telephone 410 970 2157
Preparer Fax 770 754 8036
Prepared Date 2016-03-18 00:00:00
Authorizer Name D*** L*****
Authorizer Telephone 678 762 2872
Authorizer Title Manager Phmsa Regulatory Compliance
Authorizer Email D******@c******.com
Narrative On july 6, 2015 at approximately 08:00 am, a senior operator was making rounds and noticed sheen of product inside the sting water tank access well. He notified the operations manager and lead operator of his finding. The oil water separator (ows) and sting water tank were isolated. Both the sting water tank and ows were temporarily locked out of service until repairs were complete. The sheen was collected in absorbents and the water was vacuumed up for disposal at approved recycling facility. Recovered product was less than six gallons. After further investigation by projects and environmental specialist, it was determined that the containment around the ows was not completely sealed. Although it is unlikely that the sting water breached the containment area, the determination was made to report this as potentially impacting the environment. On 7/13/15,courtesy notificationswere was made to virginia state corp commission which works on behalf of PHMSA in virginia. No other agencies were notified since it was less than 25 gallons. 3/18/2016: I was determined that the gasket on the tank valve had failed. The gasket was replaced on the tank valve; all repairs are complete.

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