Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2015-06-26 — OK
Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$500
Incident datetime
2015-06-26 12:20
Report number
Location
OK
Narrative
Heavy rainfall overnight caused excessive buildup in the facility pipe run and manifold area. The storm also knocked out electrical power to the facility for approximately one hour, preventing the pump in the product-water separator from operating. While the power was off, the rapid inflow from the storm caused the product side of the separator to fill with storm water, resulting in a leak from the gasket at the separator man-way. The co-mingled water and product was recovered with a vacuum truck and properly mitigated. The gasket was replaced, and the separator was returned to operation.
Detailed record list
Report Received Date
2015-07-24 00:00:00
Iyear
2015
Report Number
20150267
Supplemental Number
20619
Report Type
Original Final
Operator Id
22610
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2015-06-26 12:20:00
Location Latitude
39.1402
Location Longitude
-94.60133
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
0.16
Recovered Bbls
0.16
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-06-26 12:20:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Leak Was From Product-Water Separator, Which Did Not Impair Facility Operation
On Site Datetime
2015-06-26 12:20:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Kansas City Terminal
Segment Name
Terminal No. 200
Onshore State Abbreviation
Ks
Onshore Postal Code
66115-1401
Onshore City Name
Kansas City
Onshore County Name
Wyandotte
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Manway On Product-Water Separator
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Sump
Installation Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Gasket Material
Release Type
Leak
Leak Type
Other
Leak Type Other
Gasket
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
0.16
Rel Water Name
Facility Storm Water Contained On-Site
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
20
Est Cost Prop Damage
500
Est Cost Emergency
9400
Est Cost Environmental
0
Est Cost Other
0
Prpty
9920
Accident Psig
0
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Sump is locally monitored by kansas city electronic operation system, but not by scada in the tulsa operations control center.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Electricity Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Heavy Rain
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7377
Prepared Date
2015-07-24 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
Heavy rainfall overnight caused excessive buildup in the facility pipe run and manifold area. The storm also knocked out electrical power to the facility for approximately one hour, preventing the pump in the product-water separator from operating. While the power was off, the rapid inflow from the storm caused the product side of the separator to fill with storm water, resulting in a leak from the gasket at the separator man-way. The co-mingled water and product was recovered with a vacuum truck and properly mitigated. The gasket was replaced, and the separator was returned to operation.
| Report Received Date | 2015-07-24 00:00:00 |
|---|---|
| Iyear | 2015 |
| Report Number | 20150267 |
| Supplemental Number | 20619 |
| Report Type | Original Final |
| Operator Id | 22610 PHMSA Enforcement |
| Name | Magellan Pipeline Company, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2015-06-26 12:20:00 |
| Location Latitude | 39.1402 Google Maps OpenStreetMap |
| Location Longitude | -94.60133 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Mixture Of Refined Products (Transmix Or Other Mixture) |
| Unintentional Release Bbls | 0.16 |
| Recovered Bbls | 0.16 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2015-06-26 12:20:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Leak Was From Product-Water Separator, Which Did Not Impair Facility Operation |
| On Site Datetime | 2015-06-26 12:20:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Kansas City Terminal |
| Segment Name | Terminal No. 200 |
| Onshore State Abbreviation | Ks |
| Onshore Postal Code | 66115-1401 |
| Onshore City Name | Kansas City |
| Onshore County Name | Wyandotte |
| Designated Location | Milepost/valve Station |
| Designated Name | 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Other |
| Incident Area Details | Manway On Product-Water Separator |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Sump |
| Installation Year | Unknown |
| Material Involved | Material Other Than Carbon Steel |
| Material Details | Gasket Material |
| Release Type | Leak |
| Leak Type | Other |
| Leak Type Other | Gasket |
| Wildlife Impact Ind | No |
| Soil Contamination | No |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | Yes |
| Surface Contam Ind | Yes |
| Amount Released | 0.16 |
| Rel Water Name | Facility Storm Water Contained On-Site |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 20 |
| Est Cost Prop Damage | 500 |
| Est Cost Emergency | 9400 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 9920 |
| Accident Psig | 0 |
| Mop Psig | 275 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Sump is locally monitored by kansas city electronic operation system, but not by scada in the tulsa operations control center. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Other Non Threaded Ind | Gasket |
| Additional Electricity Ind | Yes |
| Eq Additional Other Ind | Yes |
| Eq Additional Other Details | Heavy Rain |
| Preparer Name | K****** L* L******* |
| Preparer Title | Sr. Compliance Coordinator |
| Preparer Email | K***********@m*********.com |
| Preparer Telephone | 918-574-7315 |
| Preparer Fax | 918-574-7377 |
| Prepared Date | 2015-07-24 00:00:00 |
| Authorizer Name | K****** L* L******* |
| Authorizer Telephone | 918-574-7315 |
| Authorizer Title | Sr. Compliance Coordinator |
| Authorizer Email | K***********@m*********.com |
| Narrative | Heavy rainfall overnight caused excessive buildup in the facility pipe run and manifold area. The storm also knocked out electrical power to the facility for approximately one hour, preventing the pump in the product-water separator from operating. While the power was off, the rapid inflow from the storm caused the product side of the separator to fill with storm water, resulting in a leak from the gasket at the separator man-way. The co-mingled water and product was recovered with a vacuum truck and properly mitigated. The gasket was replaced, and the separator was returned to operation. |
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