HL incident on 2015-06-19 — TX

Operator
West Texas Gulf Pipeline Co
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$40,000
Incident datetime
2015-06-19 23:54
Report number
Location
TX
Narrative
At 22:56 on june 19 control center received lel alarm at wortham which caused a station lockout. Controller called area supervisor to have personnel dispatched to the station to investigate. At 23:01 controller began to shut down the system. Local operating personnel arrived to the station at 23:54 and found and confirmed the release at 00:08 on june 20. The immediate apparent cause of the release was a gasket failure on an ansi 600 series flanged, 2" branch drain connection to the 10" relief line off of the inbound 26" mainline. This short branch drain connection supported a cantilevered ball valve. All product released was contained on company property primarily in two (2) retention ponds inside the station. Contaminated equipment was cleaned, contaminated soil was removed and all free product skimmed from retention ponds. Failure analysis revealed that the most likely cause of the failure was vibrational self-loosening of the flange studs of the 2" branch drain connection and the studs holding the valve body together which resulted in gasket failures at each point. The associated 10" relief line piping that contained the 2" branch drain connection was removed and replaced in november 2015 with a spool piece that does not contain a similar branch connection to prevent any future recurrence.
Detailed record list
Report Received Date
2015-07-16 00:00:00
Iyear
2015
Report Number
20150259
Supplemental Number
21265
Report Type
Supplemental Final
Operator Id
Name
West Texas Gulf Pipeline Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-06-19 22:56:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
3300
Recovered Bbls
3100
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2015-06-19 23:54:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-06-19 23:01:00
Restart Datetime
2015-06-21 00:20:00
On Site Datetime
2015-06-20 00:08:00
Nrc Rpt Datetime
2015-06-20 02:03:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wtg-Wortham Station
Segment Name
Wtg-23010-26" Colorado City To Wortham
Onshore State Abbreviation
Tx
Onshore Postal Code
76693
Onshore City Name
Wortham
Onshore County Name
Freestone
Designated Location
Milepost/valve Station
Designated Name
Mp 273
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
2013
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
3000
Rel Water Name
Wortham Station Containment/retention Ponds
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
11200
Est Cost Prop Damage
40000
Est Cost Emergency
403551
Est Cost Environmental
210000
Est Cost Other
0
Prpty
664751
Accident Psig
535
Mop Psig
588
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
Yes
Exceed Restriction Ind
No
Phmsa Restriction Ind
Phmsa
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Following release the controller on duty was drug & alcohol tested because their involvement in the cause could not initially be discounted. Additionally, an investigation into their actions was initiated. Upon discovery that the release was due to a mechanical failure and the review of the controller's reactions to the event were found to be appropriate the investigation was terminated.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
Yes
Num Employees Tested
1
Num Employees Failed
0
Num Contractors Tested
1
Num Contractors Failed
0
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Vibration Ind
Yes
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2016-03-23 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
At 22:56 on june 19 control center received lel alarm at wortham which caused a station lockout. Controller called area supervisor to have personnel dispatched to the station to investigate. At 23:01 controller began to shut down the system. Local operating personnel arrived to the station at 23:54 and found and confirmed the release at 00:08 on june 20. The immediate apparent cause of the release was a gasket failure on an ansi 600 series flanged, 2" branch drain connection to the 10" relief line off of the inbound 26" mainline. This short branch drain connection supported a cantilevered ball valve. All product released was contained on company property primarily in two (2) retention ponds inside the station. Contaminated equipment was cleaned, contaminated soil was removed and all free product skimmed from retention ponds. Failure analysis revealed that the most likely cause of the failure was vibrational self-loosening of the flange studs of the 2" branch drain connection and the studs holding the valve body together which resulted in gasket failures at each point. The associated 10" relief line piping that contained the 2" branch drain connection was removed and replaced in november 2015 with a spool piece that does not contain a similar branch connection to prevent any future recurrence.
Report Received Date 2015-07-16 00:00:00
Iyear 2015
Report Number 20150259
Supplemental Number 21265
Report Type Supplemental Final
Operator Id 22442 PHMSA Enforcement
Name West Texas Gulf Pipeline Co
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-06-19 22:56:00
Location Latitude 31.77691 Google Maps OpenStreetMap
Location Longitude -96.39599 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 3300
Recovered Bbls 3100
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2015-06-19 23:54:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-06-19 23:01:00
Restart Datetime 2015-06-21 00:20:00
On Site Datetime 2015-06-20 00:08:00
Nrc Rpt Datetime 2015-06-20 02:03:00
Nrc Rpt Num 1120366 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wtg-Wortham Station
Segment Name Wtg-23010-26" Colorado City To Wortham
Onshore State Abbreviation Tx
Onshore Postal Code 76693
Onshore City Name Wortham
Onshore County Name Freestone
Designated Location Milepost/valve Station
Designated Name Mp 273
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 2013
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Surface Water Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 3000
Rel Water Name Wortham Station Containment/retention Ponds
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 11200
Est Cost Prop Damage 40000
Est Cost Emergency 403551
Est Cost Environmental 210000
Est Cost Other 0
Prpty 664751
Accident Psig 535
Mop Psig 588
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind Yes
Exceed Restriction Ind No
Phmsa Restriction Ind Phmsa
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Following release the controller on duty was drug & alcohol tested because their involvement in the cause could not initially be discounted. Additionally, an investigation into their actions was initiated. Upon discovery that the release was due to a mechanical failure and the review of the controller's reactions to the event were found to be appropriate the investigation was terminated.
Employee Drug Test Ind Yes
Contractor Drug Test Ind Yes
Num Employees Tested 1
Num Employees Failed 0
Num Contractors Tested 1
Num Contractors Failed 0
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Vibration Ind Yes
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2016-03-23 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative At 22:56 on june 19 control center received lel alarm at wortham which caused a station lockout. Controller called area supervisor to have personnel dispatched to the station to investigate. At 23:01 controller began to shut down the system. Local operating personnel arrived to the station at 23:54 and found and confirmed the release at 00:08 on june 20. The immediate apparent cause of the release was a gasket failure on an ansi 600 series flanged, 2" branch drain connection to the 10" relief line off of the inbound 26" mainline. This short branch drain connection supported a cantilevered ball valve. All product released was contained on company property primarily in two (2) retention ponds inside the station. Contaminated equipment was cleaned, contaminated soil was removed and all free product skimmed from retention ponds. Failure analysis revealed that the most likely cause of the failure was vibrational self-loosening of the flange studs of the 2" branch drain connection and the studs holding the valve body together which resulted in gasket failures at each point. The associated 10" relief line piping that contained the 2" branch drain connection was removed and replaced in november 2015 with a spool piece that does not contain a similar branch connection to prevent any future recurrence.

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