HL incident on 2015-06-18 — TX

Operator
Nustar Logistics, L.p.
Cause
Corrosion Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$648,703
Incident datetime
2015-06-18 08:05
Report number
Location
TX
Narrative
While operating the 40p houston lpg pipeline, a pressure drop was identified. Emergency response crews began isolating mainline valves and checking immediate response areas. An aerial patrol was dispatched, and a pipeline release was discovered within a rural area of victoria county. Permanent repairs were made by replacing 60 feet of 12-inch steel pipe. Update: the failure was caused by external corrosion. The origin of the rupture was a through-wall external corrosion pit within a corrosion colony that overlapped the longitudinal seam weld of the pipe.
Detailed record list
Report Received Date
2015-07-15 00:00:00
Iyear
2015
Report Number
20150257
Supplemental Number
21377
Report Type
Supplemental Final
Operator Id
Name
Nustar Logistics, L.p.
Operator Street Address
8111 Westchester Drive
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75225
Local Datetime
2015-06-18 04:09:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
8000
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Operator Employee
Incident Identified Datetime
2015-06-18 08:05:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Prior To The Leak, The Pipeline Was Blocked In From Oneok To Midway Pump Station
On Site Datetime
2015-06-18 08:05:00
Nrc Rpt Datetime
2015-06-18 09:30:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
40p Houston Lpg Pipeline
Segment Name
Gohlke To Greta
Onshore State Abbreviation
Tx
Onshore Postal Code
77905
Onshore City Name
Not Within A Municipality
Onshore County Name
Victoria
Designated Location
Survey Station No.
Designated Name
861489
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
12.75
Pipe Wall Thickness
0.203
Pipe Smys
46000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1966
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Longitudinal
Rupture Width
31.8
Rupture Length
108
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
120000
Est Cost Gas Released
162120
Est Cost Prop Damage
648703
Est Cost Emergency
96840
Est Cost Environmental
0
Est Cost Other
14784
Est Cost Other Details
Estimated Other Costs Include Metallurgical Analysis/failure Investigation
Prpty
1042447
Accident Psig
642
Mop Psig
1050
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
27040
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control room activities did not contribute to the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
General Corrosion
Microbiological Corrosion Ind
Yes
Metallurgical Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
Unknown
Shielding Evident
Unknown
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Cp Annual Survey Year
2015
Close Interval Survey Year
2009
Prior Damage
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Cir Trn Wave Mgn Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2011
Circ Wave Recent Year
2011
Geometry Recent Year
2011
Other Recent Year
2011
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2012
Hydrtst Most Rcnt Pressure
1364
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
R****** P****
Preparer Title
Lead Pipeline Safety Specialist
Preparer Email
R************@n***********.com
Preparer Telephone
361-249-9417
Preparer Fax
210-918-7117
Prepared Date
2016-05-17 00:00:00
Authorizer Name
W** G***
Authorizer Telephone
361-249-9402
Authorizer Title
Vice President And General Manager
Authorizer Email
W*******@n***********.com
Narrative
While operating the 40p houston lpg pipeline, a pressure drop was identified. Emergency response crews began isolating mainline valves and checking immediate response areas. An aerial patrol was dispatched, and a pipeline release was discovered within a rural area of victoria county. Permanent repairs were made by replacing 60 feet of 12-inch steel pipe. Update: the failure was caused by external corrosion. The origin of the rupture was a through-wall external corrosion pit within a corrosion colony that overlapped the longitudinal seam weld of the pipe.
Report Received Date 2015-07-15 00:00:00
Iyear 2015
Report Number 20150257
Supplemental Number 21377
Report Type Supplemental Final
Operator Id 31454 PHMSA Enforcement
Name Nustar Logistics, L.p.
Operator Street Address 8111 Westchester Drive
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75225
Local Datetime 2015-06-18 04:09:00
Location Latitude 28.57446 Google Maps OpenStreetMap
Location Longitude -96.93008 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 8000
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Operator Employee
Incident Identified Datetime 2015-06-18 08:05:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Prior To The Leak, The Pipeline Was Blocked In From Oneok To Midway Pump Station
On Site Datetime 2015-06-18 08:05:00
Nrc Rpt Datetime 2015-06-18 09:30:00
Nrc Rpt Num 1120150 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name 40p Houston Lpg Pipeline
Segment Name Gohlke To Greta
Onshore State Abbreviation Tx
Onshore Postal Code 77905
Onshore City Name Not Within A Municipality
Onshore County Name Victoria
Designated Location Survey Station No.
Designated Name 861489
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 12.75
Pipe Wall Thickness 0.203
Pipe Smys 46000
Pipe Specification Api 5l
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1966
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Longitudinal
Rupture Width 31.8
Rupture Length 108
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 120000
Est Cost Gas Released 162120
Est Cost Prop Damage 648703
Est Cost Emergency 96840
Est Cost Environmental 0
Est Cost Other 14784
Est Cost Other Details Estimated Other Costs Include Metallurgical Analysis/failure Investigation
Prpty 1042447
Accident Psig 642
Mop Psig 1050
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 27040
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Control room activities did not contribute to the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results General Corrosion
Microbiological Corrosion Ind Yes
Metallurgical Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year Unknown
Shielding Evident Unknown
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Cp Annual Survey Year 2015
Close Interval Survey Year 2009
Prior Damage Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Cir Trn Wave Mgn Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2011
Circ Wave Recent Year 2011
Geometry Recent Year 2011
Other Recent Year 2011
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2012
Hydrtst Most Rcnt Pressure 1364
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name R****** P****
Preparer Title Lead Pipeline Safety Specialist
Preparer Email R************@n***********.com
Preparer Telephone 361-249-9417
Preparer Fax 210-918-7117
Prepared Date 2016-05-17 00:00:00
Authorizer Name W** G***
Authorizer Telephone 361-249-9402
Authorizer Title Vice President And General Manager
Authorizer Email W*******@n***********.com
Narrative While operating the 40p houston lpg pipeline, a pressure drop was identified. Emergency response crews began isolating mainline valves and checking immediate response areas. An aerial patrol was dispatched, and a pipeline release was discovered within a rural area of victoria county. Permanent repairs were made by replacing 60 feet of 12-inch steel pipe. Update: the failure was caused by external corrosion. The origin of the rupture was a through-wall external corrosion pit within a corrosion colony that overlapped the longitudinal seam weld of the pipe.

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