HL incident on 2015-06-01 — TX

Operator
West Texas Gulf Pipeline Co
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,000
Incident datetime
2015-06-01 11:00
Report number
Location
TX
Narrative
During a routine switch from tank #15 to tank #18 at colorado city, the mov on tank #18 failed due to a stripped valve stem nut. Therefore the valve was showing to be in the open position for scada yet was actually closed. This event triggered the manifold relief system and oil backed up the thermal relief line into an atmospheric funnel for the relief valve used for sampling and onto the concrete containment. The mov was repaired and the thermal relief valve funnel was removed and replaced with piping to the sump drain line. The system was evaluated for any additional atmospheric thermal relief valves and all valves were replaced with piping to the sump drain line.
Detailed record list
Report Received Date
2015-07-01 00:00:00
Iyear
2015
Report Number
20150239
Supplemental Number
20802
Report Type
Supplemental Final
Operator Id
Name
West Texas Gulf Pipeline Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-06-01 11:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.71
Recovered Bbls
0.71
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2015-06-01 11:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank Line Isolated.
On Site Datetime
2015-06-01 11:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wtg-Colorado City Station
Segment Name
Colorado City Station Piping
Onshore State Abbreviation
Tx
Onshore Postal Code
79526
Onshore City Name
Colorado City
Onshore County Name
Scurry
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Relief Valve
Installation Year
2000
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Thermal Relief To Containment
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
2000
Est Cost Emergency
3000
Est Cost Environmental
0
Est Cost Other
0
Prpty
5000
Accident Psig
267
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Relief Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Thermal Relief Pop-Off Valve Vented To An Atmospheric Funnel Used For Sampling R
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2015-10-06 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
During a routine switch from tank #15 to tank #18 at colorado city, the mov on tank #18 failed due to a stripped valve stem nut. Therefore the valve was showing to be in the open position for scada yet was actually closed. This event triggered the manifold relief system and oil backed up the thermal relief line into an atmospheric funnel for the relief valve used for sampling and onto the concrete containment. The mov was repaired and the thermal relief valve funnel was removed and replaced with piping to the sump drain line. The system was evaluated for any additional atmospheric thermal relief valves and all valves were replaced with piping to the sump drain line.
Report Received Date 2015-07-01 00:00:00
Iyear 2015
Report Number 20150239
Supplemental Number 20802
Report Type Supplemental Final
Operator Id 22442 PHMSA Enforcement
Name West Texas Gulf Pipeline Co
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-06-01 11:00:00
Location Latitude 32.52944 Google Maps OpenStreetMap
Location Longitude -100.83055 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.71
Recovered Bbls 0.71
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Controller
Operator Type Operator Employee
Incident Identified Datetime 2015-06-01 11:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank Line Isolated.
On Site Datetime 2015-06-01 11:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wtg-Colorado City Station
Segment Name Colorado City Station Piping
Onshore State Abbreviation Tx
Onshore Postal Code 79526
Onshore City Name Colorado City
Onshore County Name Scurry
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Relief Valve
Installation Year 2000
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Thermal Relief To Containment
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 2000
Est Cost Emergency 3000
Est Cost Environmental 0
Est Cost Other 0
Prpty 5000
Accident Psig 267
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Relief Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Thermal Relief Pop-Off Valve Vented To An Atmospheric Funnel Used For Sampling R
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2015-10-06 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative During a routine switch from tank #15 to tank #18 at colorado city, the mov on tank #18 failed due to a stripped valve stem nut. Therefore the valve was showing to be in the open position for scada yet was actually closed. This event triggered the manifold relief system and oil backed up the thermal relief line into an atmospheric funnel for the relief valve used for sampling and onto the concrete containment. The mov was repaired and the thermal relief valve funnel was removed and replaced with piping to the sump drain line. The system was evaluated for any additional atmospheric thermal relief valves and all valves were replaced with piping to the sump drain line.

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