HL incident on 2015-05-31 — TX

Operator
Sunoco Pipeline L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2015-05-31 13:29
Report number
Location
TX
Narrative
On 5/31/2015 the control center notified field operations personnel that they were unable to start the truck injection pump due to an lel alarm on the truck act. Local operations personnel were dispatched to the location and confirmed a release of crude oil in the station manifold area. Investigation revealed a pinhole in a section of deadleg station piping. The deadleg was removed from the system and a review of the station piping for any additional deadleg piping was conducted. Subsequent to the review of diboll station, all deadleg piping within the station has been removed.
Detailed record list
Report Received Date
2015-06-30 00:00:00
Iyear
2015
Report Number
20150238
Supplemental Number
21063
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-05-31 13:29:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
60
Recovered Bbls
50
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-05-31 13:29:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Segment Down Per Schedule
On Site Datetime
2015-05-31 13:29:00
Nrc Rpt Datetime
2015-05-31 17:36:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Diboll Station
Segment Name
Station Manifold Piping
Onshore State Abbreviation
Tx
Onshore Postal Code
75941
Onshore City Name
Diboll
Onshore County Name
Angelina
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8.625
Pipe Wall Thickness
0.322
Pipe Smys
35000
Pipe Specification
Api 5l
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
1963
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
568
Est Cost Prop Damage
5000
Est Cost Emergency
21488
Est Cost Environmental
100000
Est Cost Other
0
Prpty
127056
Accident Psig
50
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Other Basis Ind
Yes
Int Corrosion Basis Details
Visual Assessment By Laboratory
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2016-01-19 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
On 5/31/2015 the control center notified field operations personnel that they were unable to start the truck injection pump due to an lel alarm on the truck act. Local operations personnel were dispatched to the location and confirmed a release of crude oil in the station manifold area. Investigation revealed a pinhole in a section of deadleg station piping. The deadleg was removed from the system and a review of the station piping for any additional deadleg piping was conducted. Subsequent to the review of diboll station, all deadleg piping within the station has been removed.
Report Received Date 2015-06-30 00:00:00
Iyear 2015
Report Number 20150238
Supplemental Number 21063
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-05-31 13:29:00
Location Latitude 31.15918 Google Maps OpenStreetMap
Location Longitude -94.6758 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 60
Recovered Bbls 50
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-05-31 13:29:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Segment Down Per Schedule
On Site Datetime 2015-05-31 13:29:00
Nrc Rpt Datetime 2015-05-31 17:36:00
Nrc Rpt Num 1118191 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Diboll Station
Segment Name Station Manifold Piping
Onshore State Abbreviation Tx
Onshore Postal Code 75941
Onshore City Name Diboll
Onshore County Name Angelina
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8.625
Pipe Wall Thickness 0.322
Pipe Smys 35000
Pipe Specification Api 5l
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year 1963
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 568
Est Cost Prop Damage 5000
Est Cost Emergency 21488
Est Cost Environmental 100000
Est Cost Other 0
Prpty 127056
Accident Psig 50
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Other Basis Ind Yes
Int Corrosion Basis Details Visual Assessment By Laboratory
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Manager
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 877-917-0448
Prepared Date 2016-01-19 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Manager
Authorizer Email T*********@s**************.com
Narrative On 5/31/2015 the control center notified field operations personnel that they were unable to start the truck injection pump due to an lel alarm on the truck act. Local operations personnel were dispatched to the location and confirmed a release of crude oil in the station manifold area. Investigation revealed a pinhole in a section of deadleg station piping. The deadleg was removed from the system and a review of the station piping for any additional deadleg piping was conducted. Subsequent to the review of diboll station, all deadleg piping within the station has been removed.

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