Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2015-05-31 — TX
Operator
Sunoco Pipeline L.p.
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$5,000
Incident datetime
2015-05-31 13:29
Report number
Location
TX
Narrative
On 5/31/2015 the control center notified field operations personnel that they were unable to start the truck injection pump due to an lel alarm on the truck act. Local operations personnel were dispatched to the location and confirmed a release of crude oil in the station manifold area. Investigation revealed a pinhole in a section of deadleg station piping. The deadleg was removed from the system and a review of the station piping for any additional deadleg piping was conducted. Subsequent to the review of diboll station, all deadleg piping within the station has been removed.
Detailed record list
Report Received Date
2015-06-30 00:00:00
Iyear
2015
Report Number
20150238
Supplemental Number
21063
Report Type
Supplemental Final
Operator Id
18718
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-05-31 13:29:00
Location Latitude
31.15918
Location Longitude
-94.6758
Commodity Released Type
Crude Oil
Unintentional Release Bbls
60
Recovered Bbls
50
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-05-31 13:29:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Segment Down Per Schedule
On Site Datetime
2015-05-31 13:29:00
Nrc Rpt Datetime
2015-05-31 17:36:00
Nrc Rpt Num
1118191
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Diboll Station
Segment Name
Station Manifold Piping
Onshore State Abbreviation
Tx
Onshore Postal Code
75941
Onshore City Name
Diboll
Onshore County Name
Angelina
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8.625
Pipe Wall Thickness
0.322
Pipe Smys
35000
Pipe Specification
Api 5l
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
1963
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
568
Est Cost Prop Damage
5000
Est Cost Emergency
21488
Est Cost Environmental
100000
Est Cost Other
0
Prpty
127056
Accident Psig
50
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Other Basis Ind
Yes
Int Corrosion Basis Details
Visual Assessment By Laboratory
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Manager
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
877-917-0448
Prepared Date
2016-01-19 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Manager
Authorizer Email
T*********@s**************.com
Narrative
On 5/31/2015 the control center notified field operations personnel that they were unable to start the truck injection pump due to an lel alarm on the truck act. Local operations personnel were dispatched to the location and confirmed a release of crude oil in the station manifold area. Investigation revealed a pinhole in a section of deadleg station piping. The deadleg was removed from the system and a review of the station piping for any additional deadleg piping was conducted. Subsequent to the review of diboll station, all deadleg piping within the station has been removed.
| Report Received Date | 2015-06-30 00:00:00 |
|---|---|
| Iyear | 2015 |
| Report Number | 20150238 |
| Supplemental Number | 21063 |
| Report Type | Supplemental Final |
| Operator Id | 18718 PHMSA Enforcement |
| Name | Sunoco Pipeline L.p. |
| Operator Street Address | 1300 Main Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2015-05-31 13:29:00 |
| Location Latitude | 31.15918 Google Maps OpenStreetMap |
| Location Longitude | -94.6758 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 60 |
| Recovered Bbls | 50 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2015-05-31 13:29:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Line Segment Down Per Schedule |
| On Site Datetime | 2015-05-31 13:29:00 |
| Nrc Rpt Datetime | 2015-05-31 17:36:00 |
| Nrc Rpt Num | 1118191 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Diboll Station |
| Segment Name | Station Manifold Piping |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 75941 |
| Onshore City Name | Diboll |
| Onshore County Name | Angelina |
| Designated Location | Survey Station No. |
| Designated Name | 0+00 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Soil |
| Depth Of Cover | 36 |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Pipe |
| Pipe Type | Pipe Body |
| Pipe Diameter | 8.625 |
| Pipe Wall Thickness | 0.322 |
| Pipe Smys | 35000 |
| Pipe Specification | Api 5l |
| Pipe Seam Type | Seamless |
| Pipe Manufacturer | Unknown |
| Pipe Coating Type | Fusion Bonded Epoxy(Fbe) |
| Installation Year | 1963 |
| Manufactured Year | Unknown |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Pinhole |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 568 |
| Est Cost Prop Damage | 5000 |
| Est Cost Emergency | 21488 |
| Est Cost Environmental | 100000 |
| Est Cost Other | 0 |
| Prpty | 127056 |
| Accident Psig | 50 |
| Mop Psig | 285 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | Yes |
| Scada Conf Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | A review of the accident determined that there were no control room actions that contributed to the event. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Corrosion Failure |
| Cause Details | Internal Corrosion |
| Internal External | Internal Corrosion |
| Int Visual Exam Results | Localized Pitting |
| Int Microbiological Ind | Yes |
| Int Other Basis Ind | Yes |
| Int Corrosion Basis Details | Visual Assessment By Laboratory |
| Int Low Point Pipe Loc Ind | Yes |
| Corrosion Inhibitors | Yes |
| Corrosion Lining | No |
| Cleaning Dewatering | Not Applicable - Not Mainline Pipe |
| Corrosion Coupons | Not Applicable - Not Mainline Pipe |
| Collected Data Ind | No |
| Has Hydrtst Conduc Before Ind | No |
| Direct Asmnt Conducted | No |
| Non Destructive Exam Ind | No |
| Preparer Name | T*** G* N******* |
| Preparer Title | Dot Compliance Manager |
| Preparer Email | T*********@s**************.com |
| Preparer Telephone | 281-637-6576 |
| Preparer Fax | 877-917-0448 |
| Prepared Date | 2016-01-19 00:00:00 |
| Authorizer Name | T*** G* N******* |
| Authorizer Telephone | 281-637-6576 |
| Authorizer Title | Dot Compliance Manager |
| Authorizer Email | T*********@s**************.com |
| Narrative | On 5/31/2015 the control center notified field operations personnel that they were unable to start the truck injection pump due to an lel alarm on the truck act. Local operations personnel were dispatched to the location and confirmed a release of crude oil in the station manifold area. Investigation revealed a pinhole in a section of deadleg station piping. The deadleg was removed from the system and a review of the station piping for any additional deadleg piping was conducted. Subsequent to the review of diboll station, all deadleg piping within the station has been removed. |
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