HL incident on 2015-05-28 — TX

Operator
Energy Transfer Company
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2015-05-28 13:00
Report number
Location
TX
Narrative
In the process of installing a valve setting for a new pump station, a section of pipe was stoppled and bypassed in the halley 5 acre yard. The stopples had been installed and the section of pipe between the bypass was taken out of service. The pipe was cut loose and the weld was completed on the upstream side. After the weld was made, a leak was discovered on the downstream stopple. The control room and the upstream plants were notified and the pipeline was shut in for safety reasons.
Detailed record list
Report Received Date
2015-06-26 00:00:00
Iyear
2015
Report Number
20150235
Supplemental Number
20555
Report Type
Original Final
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-05-28 13:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.5
Intentional Release Bbls
90
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-05-28 13:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-05-28 13:30:00
Restart Datetime
2015-05-29 02:00:00
On Site Datetime
2015-05-28 13:00:00
Nrc Rpt Datetime
2015-05-28 14:30:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Txbw1p2c
Segment Name
Halley Pegasus Junction
Onshore State Abbreviation
Tx
Onshore Postal Code
79745
Onshore City Name
Kermit
Onshore County Name
Winkler
Designated Location
Survey Station No.
Designated Name
734+63
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
76
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tap Fitting(Stopple, Thread-O-Ring, Weld-O-Let, Etc.)
Installation Year
2015
Material Involved
Material Other Than Carbon Steel
Material Details
Stopple Fitting Component.
Release Type
Leak
Leak Type
Other
Leak Type Other
Stopple Fitting Component.
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1500
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
1500
Accident Psig
806
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
415
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
The Segment That The Leak Occurred On Was Station Piping.
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak was on a stopple fitting component.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Stopple Control Fitting Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Stopple Fitting Component.
Preparer Name
N***** H******
Preparer Title
Director - Regulatory Compliance
Preparer Email
N*************@e*************.com
Preparer Telephone
7138575479
Prepared Date
2015-06-26 00:00:00
Authorizer Name
N***** H******
Authorizer Telephone
7138575479
Authorizer Title
Director - Regulatory Compliance
Authorizer Email
N*************@e*************.com
Narrative
In the process of installing a valve setting for a new pump station, a section of pipe was stoppled and bypassed in the halley 5 acre yard. The stopples had been installed and the section of pipe between the bypass was taken out of service. The pipe was cut loose and the weld was completed on the upstream side. After the weld was made, a leak was discovered on the downstream stopple. The control room and the upstream plants were notified and the pipeline was shut in for safety reasons.
Report Received Date 2015-06-26 00:00:00
Iyear 2015
Report Number 20150235
Supplemental Number 20555
Report Type Original Final
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-05-28 13:30:00
Location Latitude 31.7316 Google Maps OpenStreetMap
Location Longitude -102.988 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 0.5
Intentional Release Bbls 90
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-05-28 13:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-05-28 13:30:00
Restart Datetime 2015-05-29 02:00:00
On Site Datetime 2015-05-28 13:00:00
Nrc Rpt Datetime 2015-05-28 14:30:00
Nrc Rpt Num 1117866 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Txbw1p2c
Segment Name Halley Pegasus Junction
Onshore State Abbreviation Tx
Onshore Postal Code 79745
Onshore City Name Kermit
Onshore County Name Winkler
Designated Location Survey Station No.
Designated Name 734+63
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 76
Crossing No
Pipe Facility Type Interstate
Item Involved Tap Fitting(Stopple, Thread-O-Ring, Weld-O-Let, Etc.)
Installation Year 2015
Material Involved Material Other Than Carbon Steel
Material Details Stopple Fitting Component.
Release Type Leak
Leak Type Other
Leak Type Other Stopple Fitting Component.
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1500
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 1500
Accident Psig 806
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 415
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details The Segment That The Leak Occurred On Was Station Piping.
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The leak was on a stopple fitting component.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Stopple Control Fitting Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Stopple Fitting Component.
Preparer Name N***** H******
Preparer Title Director - Regulatory Compliance
Preparer Email N*************@e*************.com
Preparer Telephone 7138575479
Prepared Date 2015-06-26 00:00:00
Authorizer Name N***** H******
Authorizer Telephone 7138575479
Authorizer Title Director - Regulatory Compliance
Authorizer Email N*************@e*************.com
Narrative In the process of installing a valve setting for a new pump station, a section of pipe was stoppled and bypassed in the halley 5 acre yard. The stopples had been installed and the section of pipe between the bypass was taken out of service. The pipe was cut loose and the weld was completed on the upstream side. After the weld was made, a leak was discovered on the downstream stopple. The control room and the upstream plants were notified and the pipeline was shut in for safety reasons.

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