HL incident on 2015-06-07 — TX

Operator
Shell Pipeline Co., L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2015-06-07 20:53
Report number
Location
TX
Narrative
The control center received an indication from a mainline pump station for the hydro carbon monitor. The controller took action and shut down the pipeline system, isolated the station, called the on call operations personnel to investigate. The operations personnel found the pump station discharge block valve stem had released crude oil to the ground. Contacted mechanic to inspect valve and valve stem packing. Valve stem packing added. Clean up of crude oil to soil and hydro carbon monitor. Returned pipeline to service at 02:35 6/8/15. Updated volume from .24 to .6 bbls. From clean up contractor. Questions from PHMSA - valve inspection records. - notification to nrc. Control center received an indication of hydrocarbon monitor, controller shut down pipeline and isolated pump station. The indications have sometimes been false alarms. Sent out on-call operator investigate. Drive to pump station in heavy rain storm was one hour and ten minutes. Found evidence of release, contacted control center & operations supervisor, time 22:40. Operations supervisor contacted emergency response representative with information of incident. Emergency response representative made the call to the nrc at 23:23.
Detailed record list
Report Received Date
2015-06-26 00:00:00
Iyear
2015
Report Number
20150234
Supplemental Number
21081
Report Type
Supplemental Final
Operator Id
Name
Shell Pipeline Co., L.p.
Operator Street Address
150 North Dairy Ashford Road Wck Bldg. A
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2015-06-07 20:53:00
Location Latitude
Location Longitude
-91.65165833
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.6
Recovered Bbls
0.6
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2015-06-07 20:53:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-06-07 20:54:00
Restart Datetime
2015-06-08 02:35:00
On Site Datetime
2015-06-07 22:40:00
Nrc Rpt Datetime
2015-06-07 23:23:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Julien Pump Station
Segment Name
Erath - Houma 22"
Onshore State Abbreviation
La
Onshore Postal Code
70514
Onshore City Name
Not Within A Municipality
Onshore County Name
St. Mary
Designated Location
Milepost/valve Station
Designated Name
Julien Pmp St
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Orion
Installation Year
2013
Manufactured Year
2012
Material Involved
Material Other Than Carbon Steel
Material Details
Stem Packing
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
500
Est Cost Emergency
4500
Est Cost Environmental
0
Est Cost Other
0
Prpty
5000
Accident Psig
487
Mop Psig
849
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller's response to the alarm was in a timely manner and the shutdown was executed per procedure.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Block Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Valve Stem Packing
Preparer Name
R****** K*****
Preparer Title
Regulatory Specialist
Preparer Email
R*************@s****.com
Preparer Telephone
713 241 1064
Preparer Fax
713 241 8498
Prepared Date
2016-01-28 00:00:00
Authorizer Name
D****** P****
Authorizer Telephone
713 241 2035
Authorizer Title
Integrity And Regulatoyr Srvc Mngr
Authorizer Email
D************@s****.com
Narrative
The control center received an indication from a mainline pump station for the hydro carbon monitor. The controller took action and shut down the pipeline system, isolated the station, called the on call operations personnel to investigate. The operations personnel found the pump station discharge block valve stem had released crude oil to the ground. Contacted mechanic to inspect valve and valve stem packing. Valve stem packing added. Clean up of crude oil to soil and hydro carbon monitor. Returned pipeline to service at 02:35 6/8/15. Updated volume from .24 to .6 bbls. From clean up contractor. Questions from PHMSA - valve inspection records. - notification to nrc. Control center received an indication of hydrocarbon monitor, controller shut down pipeline and isolated pump station. The indications have sometimes been false alarms. Sent out on-call operator investigate. Drive to pump station in heavy rain storm was one hour and ten minutes. Found evidence of release, contacted control center & operations supervisor, time 22:40. Operations supervisor contacted emergency response representative with information of incident. Emergency response representative made the call to the nrc at 23:23.
Report Received Date 2015-06-26 00:00:00
Iyear 2015
Report Number 20150234
Supplemental Number 21081
Report Type Supplemental Final
Operator Id 31174 PHMSA Enforcement
Name Shell Pipeline Co., L.p.
Operator Street Address 150 North Dairy Ashford Road Wck Bldg. A
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2015-06-07 20:53:00
Location Latitude 29.84692774 Google Maps OpenStreetMap
Location Longitude -91.65165833 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.6
Recovered Bbls 0.6
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Controller
Operator Type Operator Employee
Incident Identified Datetime 2015-06-07 20:53:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-06-07 20:54:00
Restart Datetime 2015-06-08 02:35:00
On Site Datetime 2015-06-07 22:40:00
Nrc Rpt Datetime 2015-06-07 23:23:00
Nrc Rpt Num 1119007 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Julien Pump Station
Segment Name Erath - Houma 22"
Onshore State Abbreviation La
Onshore Postal Code 70514
Onshore City Name Not Within A Municipality
Onshore County Name St. Mary
Designated Location Milepost/valve Station
Designated Name Julien Pmp St
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Orion
Installation Year 2013
Manufactured Year 2012
Material Involved Material Other Than Carbon Steel
Material Details Stem Packing
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 500
Est Cost Emergency 4500
Est Cost Environmental 0
Est Cost Other 0
Prpty 5000
Accident Psig 487
Mop Psig 849
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controller's response to the alarm was in a timely manner and the shutdown was executed per procedure.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Block Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Valve Stem Packing
Preparer Name R****** K*****
Preparer Title Regulatory Specialist
Preparer Email R*************@s****.com
Preparer Telephone 713 241 1064
Preparer Fax 713 241 8498
Prepared Date 2016-01-28 00:00:00
Authorizer Name D****** P****
Authorizer Telephone 713 241 2035
Authorizer Title Integrity And Regulatoyr Srvc Mngr
Authorizer Email D************@s****.com
Narrative The control center received an indication from a mainline pump station for the hydro carbon monitor. The controller took action and shut down the pipeline system, isolated the station, called the on call operations personnel to investigate. The operations personnel found the pump station discharge block valve stem had released crude oil to the ground. Contacted mechanic to inspect valve and valve stem packing. Valve stem packing added. Clean up of crude oil to soil and hydro carbon monitor. Returned pipeline to service at 02:35 6/8/15. Updated volume from .24 to .6 bbls. From clean up contractor. Questions from PHMSA - valve inspection records. - notification to nrc. Control center received an indication of hydrocarbon monitor, controller shut down pipeline and isolated pump station. The indications have sometimes been false alarms. Sent out on-call operator investigate. Drive to pump station in heavy rain storm was one hour and ten minutes. Found evidence of release, contacted control center & operations supervisor, time 22:40. Operations supervisor contacted emergency response representative with information of incident. Emergency response representative made the call to the nrc at 23:23.

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