HL incident on 2015-06-05 — GA

Operator
Colonial Pipeline Co
Cause
Other Accident Cause
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2015-06-05 08:20
Report number
Location
GA
Narrative
On june 5, 2015, the operator arrived to perform tank loading procedure for fsii. Upon conducting the yard inspection, he noticed a strong odor of gasoline and discovered the drip from the cooling tubing of unit 2 pump. The operator notified the lead operator and operations manager of finding at 08:30. Initial notifications were made to state and local agencies at 10:00. Based on the rate of the drip, it was estimated that the leak started about 36 hours prior to the 08:20 finding on june 5, 2015. The cooling tubing is used to divert a small volume of product through a 5/8" tubing to cool the unit motor bearings and re-inject the product into the main line. Unit 2 was isolated by local operator and the technician replaced the tubing with flexible steel hose as directed by engineering. Final cleanup ended around 18:00 on the june 5, 2015. Colonial's oil spill response organization (osro) and contractors were immediately contacted and they responded with men, equipment, sorbent pads, hand tools and empty waste containment drums. The product that leaked was fully contained in an excavation area created on april 27, 2015. Approximately 27 gallons of free product was collected by absorbents off water in the excavation area. A total of 871 gallons of water was removed from the excavation area and transported to reco biotechnology in richmond, va for recycling. Approximately 2400 pounds of soil was excavated to six waste collection drums for off-site disposal at reco biotechnologies. Based on laboratory analysis, approximately one half of a gallon of product was recovered in the soil. One drum of petroleum contaminated absorbents was collected for off-site disposal at reco biotechnology in richmond, va (reco). It was determined that the tubing failed because it was subject to high amplitude low cycle fatigue. The interim repair of the flexible steel hose will be final solution as replacement for the tubing
Detailed record list
Report Received Date
2015-06-25 00:00:00
Iyear
2015
Report Number
20150233
Supplemental Number
21432
Report Type
Supplemental Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1000 Lake St.
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009
Local Datetime
2015-06-05 08:20:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.67
Recovered Bbls
0.67
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-06-05 08:20:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Unit (#2) Was Not Running At The Time Of The Incident
On Site Datetime
2015-06-05 08:20:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Yorktown Junction
Segment Name
Line 27
Onshore State Abbreviation
Va
Onshore Postal Code
23185
Onshore City Name
Williamsburg
Onshore County Name
James City
Designated Location
Survey Station No.
Designated Name
Loc #0926
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
2015
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
100
Est Cost Emergency
8500
Est Cost Environmental
1000
Est Cost Other
2000
Est Cost Other Details
Soil Transportation And Disposal
Prpty
11700
Accident Psig
1090
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The tubing leak was not from actions nor from inactions by the controller operating the line during the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Miscellaneous
Other Type
Miscellaneous
Misc Details
It Was Determined That The Tubing Failed Because It Was Subject To High Amplitude Low Cycle Fatigue.
Preparer Name
A**** S****
Preparer Title
Compliance Coordinator
Preparer Email
A******@c******.com
Preparer Telephone
410 970 2157
Preparer Fax
770 754 8036
Prepared Date
2016-06-10 00:00:00
Authorizer Name
D*** L*****
Authorizer Telephone
678 762 2872
Authorizer Title
Manager - Phmsa Regulatory Compiance
Authorizer Email
D******@c******.com
Narrative
On june 5, 2015, the operator arrived to perform tank loading procedure for fsii. Upon conducting the yard inspection, he noticed a strong odor of gasoline and discovered the drip from the cooling tubing of unit 2 pump. The operator notified the lead operator and operations manager of finding at 08:30. Initial notifications were made to state and local agencies at 10:00. Based on the rate of the drip, it was estimated that the leak started about 36 hours prior to the 08:20 finding on june 5, 2015. The cooling tubing is used to divert a small volume of product through a 5/8" tubing to cool the unit motor bearings and re-inject the product into the main line. Unit 2 was isolated by local operator and the technician replaced the tubing with flexible steel hose as directed by engineering. Final cleanup ended around 18:00 on the june 5, 2015. Colonial's oil spill response organization (osro) and contractors were immediately contacted and they responded with men, equipment, sorbent pads, hand tools and empty waste containment drums. The product that leaked was fully contained in an excavation area created on april 27, 2015. Approximately 27 gallons of free product was collected by absorbents off water in the excavation area. A total of 871 gallons of water was removed from the excavation area and transported to reco biotechnology in richmond, va for recycling. Approximately 2400 pounds of soil was excavated to six waste collection drums for off-site disposal at reco biotechnologies. Based on laboratory analysis, approximately one half of a gallon of product was recovered in the soil. One drum of petroleum contaminated absorbents was collected for off-site disposal at reco biotechnology in richmond, va (reco). It was determined that the tubing failed because it was subject to high amplitude low cycle fatigue. The interim repair of the flexible steel hose will be final solution as replacement for the tubing
Report Received Date 2015-06-25 00:00:00
Iyear 2015
Report Number 20150233
Supplemental Number 21432
Report Type Supplemental Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1000 Lake St.
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009
Local Datetime 2015-06-05 08:20:00
Location Latitude 37.202167 Google Maps OpenStreetMap
Location Longitude -76.605211 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.67
Recovered Bbls 0.67
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-06-05 08:20:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Unit (#2) Was Not Running At The Time Of The Incident
On Site Datetime 2015-06-05 08:20:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Yorktown Junction
Segment Name Line 27
Onshore State Abbreviation Va
Onshore Postal Code 23185
Onshore City Name Williamsburg
Onshore County Name James City
Designated Location Survey Station No.
Designated Name Loc #0926
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year 2015
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 100
Est Cost Emergency 8500
Est Cost Environmental 1000
Est Cost Other 2000
Est Cost Other Details Soil Transportation And Disposal
Prpty 11700
Accident Psig 1090
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The tubing leak was not from actions nor from inactions by the controller operating the line during the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Miscellaneous
Other Type Miscellaneous
Misc Details It Was Determined That The Tubing Failed Because It Was Subject To High Amplitude Low Cycle Fatigue.
Preparer Name A**** S****
Preparer Title Compliance Coordinator
Preparer Email A******@c******.com
Preparer Telephone 410 970 2157
Preparer Fax 770 754 8036
Prepared Date 2016-06-10 00:00:00
Authorizer Name D*** L*****
Authorizer Telephone 678 762 2872
Authorizer Title Manager - Phmsa Regulatory Compiance
Authorizer Email D******@c******.com
Narrative On june 5, 2015, the operator arrived to perform tank loading procedure for fsii. Upon conducting the yard inspection, he noticed a strong odor of gasoline and discovered the drip from the cooling tubing of unit 2 pump. The operator notified the lead operator and operations manager of finding at 08:30. Initial notifications were made to state and local agencies at 10:00. Based on the rate of the drip, it was estimated that the leak started about 36 hours prior to the 08:20 finding on june 5, 2015. The cooling tubing is used to divert a small volume of product through a 5/8" tubing to cool the unit motor bearings and re-inject the product into the main line. Unit 2 was isolated by local operator and the technician replaced the tubing with flexible steel hose as directed by engineering. Final cleanup ended around 18:00 on the june 5, 2015. Colonial's oil spill response organization (osro) and contractors were immediately contacted and they responded with men, equipment, sorbent pads, hand tools and empty waste containment drums. The product that leaked was fully contained in an excavation area created on april 27, 2015. Approximately 27 gallons of free product was collected by absorbents off water in the excavation area. A total of 871 gallons of water was removed from the excavation area and transported to reco biotechnology in richmond, va for recycling. Approximately 2400 pounds of soil was excavated to six waste collection drums for off-site disposal at reco biotechnologies. Based on laboratory analysis, approximately one half of a gallon of product was recovered in the soil. One drum of petroleum contaminated absorbents was collected for off-site disposal at reco biotechnology in richmond, va (reco). It was determined that the tubing failed because it was subject to high amplitude low cycle fatigue. The interim repair of the flexible steel hose will be final solution as replacement for the tubing

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