HL incident on 2015-05-25 — TX

Operator
Shell Pipeline Co., L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000,000
Incident datetime
2015-05-25 07:33
Report number
Location
TX
Narrative
The control center commanded the pump unit to shut down during hydraulic rate modifications on the pipeline. The control center received alarms of the units continuing to run. The control center shut down the pipeline system and contacted field personnel to investigate. Failure of the esd system rendered the control equipment non functional due to loss of 48 volt power system and the back up energy storage device failed to open power contact to the motor starter of the pump units, which would have shut down the pump motor. Barriers have been added to the 48 vdc system, revised the plc logic, added fail safe features, will use the sf6 sub-station breaker as a secondary control barrier. Pipeline re-started with the pump station bypassed until repairs were completed. The pump station was restarted on june 17th with the barriers installed.
Detailed record list
Report Received Date
2015-06-24 00:00:00
Iyear
2015
Report Number
20150229
Supplemental Number
20618
Report Type
Supplemental Final
Operator Id
Name
Shell Pipeline Co., L.p.
Operator Street Address
150 North Dairy Ashford Road Wck Bldg. A
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2015-05-25 07:33:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
7.86
Recovered Bbls
1.66
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2015-05-25 07:33:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-05-25 07:39:00
Restart Datetime
2015-05-25 21:30:00
On Site Datetime
2015-05-25 09:00:00
Nrc Rpt Datetime
2015-05-25 09:02:00
Nrc Rpt Num
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Tracy Pump Station
Segment Name
North 20" Carneras To Coalinga
Onshore State Abbreviation
Ca
Onshore Postal Code
95377
Onshore City Name
Tracy
Onshore County Name
San Joaquin
Designated Location
Milepost/valve Station
Designated Name
Pump Sta.
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pump
Installation Year
1969
Material Involved
Material Other Than Carbon Steel
Material Details
Esd Equipment
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
340
Est Cost Prop Damage
1000000
Est Cost Emergency
5000
Est Cost Environmental
0
Est Cost Other
0
Prpty
1005340
Accident Psig
874
Mop Psig
912
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Esd System Failure Ind
Yes
Additional Electricity Ind
Yes
Preparer Name
R****** K*****
Preparer Title
Regulatory Specialist
Preparer Email
R*************@s****.com
Preparer Telephone
713 241 1064
Preparer Fax
713 241 8498
Prepared Date
2015-07-24 00:00:00
Authorizer Name
D****** P****
Authorizer Telephone
713 241 2035
Authorizer Title
Integrity Regulatory Srvc Manager
Authorizer Email
D************@s****.com
Narrative
The control center commanded the pump unit to shut down during hydraulic rate modifications on the pipeline. The control center received alarms of the units continuing to run. The control center shut down the pipeline system and contacted field personnel to investigate. Failure of the esd system rendered the control equipment non functional due to loss of 48 volt power system and the back up energy storage device failed to open power contact to the motor starter of the pump units, which would have shut down the pump motor. Barriers have been added to the 48 vdc system, revised the plc logic, added fail safe features, will use the sf6 sub-station breaker as a secondary control barrier. Pipeline re-started with the pump station bypassed until repairs were completed. The pump station was restarted on june 17th with the barriers installed.
Report Received Date 2015-06-24 00:00:00
Iyear 2015
Report Number 20150229
Supplemental Number 20618
Report Type Supplemental Final
Operator Id 31174 PHMSA Enforcement
Name Shell Pipeline Co., L.p.
Operator Street Address 150 North Dairy Ashford Road Wck Bldg. A
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2015-05-25 07:33:00
Location Latitude 37.721661 Google Maps OpenStreetMap
Location Longitude -121.54831 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 7.86
Recovered Bbls 1.66
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Controller
Operator Type Operator Employee
Incident Identified Datetime 2015-05-25 07:33:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-05-25 07:39:00
Restart Datetime 2015-05-25 21:30:00
On Site Datetime 2015-05-25 09:00:00
Nrc Rpt Datetime 2015-05-25 09:02:00
Nrc Rpt Num 1117471 NRC Report How to search
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Tracy Pump Station
Segment Name North 20" Carneras To Coalinga
Onshore State Abbreviation Ca
Onshore Postal Code 95377
Onshore City Name Tracy
Onshore County Name San Joaquin
Designated Location Milepost/valve Station
Designated Name Pump Sta.
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pump
Installation Year 1969
Material Involved Material Other Than Carbon Steel
Material Details Esd Equipment
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 340
Est Cost Prop Damage 1000000
Est Cost Emergency 5000
Est Cost Environmental 0
Est Cost Other 0
Prpty 1005340
Accident Psig 874
Mop Psig 912
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Esd System Failure Ind Yes
Additional Electricity Ind Yes
Preparer Name R****** K*****
Preparer Title Regulatory Specialist
Preparer Email R*************@s****.com
Preparer Telephone 713 241 1064
Preparer Fax 713 241 8498
Prepared Date 2015-07-24 00:00:00
Authorizer Name D****** P****
Authorizer Telephone 713 241 2035
Authorizer Title Integrity Regulatory Srvc Manager
Authorizer Email D************@s****.com
Narrative The control center commanded the pump unit to shut down during hydraulic rate modifications on the pipeline. The control center received alarms of the units continuing to run. The control center shut down the pipeline system and contacted field personnel to investigate. Failure of the esd system rendered the control equipment non functional due to loss of 48 volt power system and the back up energy storage device failed to open power contact to the motor starter of the pump units, which would have shut down the pump motor. Barriers have been added to the 48 vdc system, revised the plc logic, added fail safe features, will use the sf6 sub-station breaker as a secondary control barrier. Pipeline re-started with the pump station bypassed until repairs were completed. The pump station was restarted on june 17th with the barriers installed.

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