HL incident on 2015-05-20 — TX

Operator
Dcp Midstream
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,000
Incident datetime
2015-05-20 18:31
Report number
Location
TX
Narrative
On may 20, 2015 at approximately 6:30 pm, dcp was delivering to a customer who had operational issues and backed up pressure to dcp's three rivers meter skid. The shutdown valve esd 100 went closed at its set point for opp of 1350 psig. An ngl technician responded on site at approximately 7:30 pm and diverted flow to an alternate customer. Another ngl technician was called to the site for assistance and arrived at approximately 9:00 pm. When the two technicians were ready to leave at 10:10 pm, they noticed the downstream side of a relief valve was iced over. The relief valve was discharging through the vent system which is connected to the plant (customer) flare. The relief valve was stuck in the open position, so the technician then isolated and closed psv 200. After reviewing data trends, it was determined the relief valve had opened and did not reseat. The estimated time frame that the relief valve was discharging is approximately 4 hours. The estimated volume that was released is approx. 770 bbls. The relief valve was replaced on may 22, 2015. The relief valve that malfunctioned is being sent to the vendor for a failure analysis. Vendor analysis on 6/17/2015 concluded that there was a piece of welding slag between the disc and nozzle seat. This would account for the valve failing to reseat. The source of the welding slag is unknown.
Detailed record list
Report Received Date
2015-06-17 00:00:00
Iyear
2015
Report Number
20150223
Supplemental Number
20552
Report Type
Supplemental Final
Operator Id
Name
Dcp Midstream
Operator Street Address
2331 Citywest Blvd. Hq-08-S812-02
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77042
Local Datetime
2015-05-20 18:31:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
770
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2015-05-20 18:31:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Psv In Question Was Isolated And Replaced.
On Site Datetime
2015-05-20 19:30:00
Nrc Rpt Datetime
2015-05-20 22:45:00
Nrc Rpt Num
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Three Rivers Meter Station
Segment Name
Sahi-1-4
Onshore State Abbreviation
Tx
Onshore Postal Code
78022
Onshore City Name
George West
Onshore County Name
Live Oak
Designated Location
Milepost/valve Station
Designated Name
Three Rivers
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Relief Valve
Installation Year
2013
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Psv Failed To Reseat.
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
30000
Est Cost Prop Damage
2000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
32000
Accident Psig
1350
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The scada system and controller acted correctly in the situation.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Relief Valve Ind
Yes
Additional Defect Ind
Yes
Additional Installation Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Piece Of Welding Slag Found In Between The Seats
Preparer Name
T**** S******
Preparer Title
Pipeline Compliance Specialist
Preparer Email
T*******@d***********.com
Preparer Telephone
713-268-7447
Prepared Date
2015-06-25 00:00:00
Authorizer Name
B****** P*****
Authorizer Telephone
713-268-7400
Authorizer Title
Director Liquid Pipeline Compliance
Authorizer Email
B*******@d***********.com
Narrative
On may 20, 2015 at approximately 6:30 pm, dcp was delivering to a customer who had operational issues and backed up pressure to dcp's three rivers meter skid. The shutdown valve esd 100 went closed at its set point for opp of 1350 psig. An ngl technician responded on site at approximately 7:30 pm and diverted flow to an alternate customer. Another ngl technician was called to the site for assistance and arrived at approximately 9:00 pm. When the two technicians were ready to leave at 10:10 pm, they noticed the downstream side of a relief valve was iced over. The relief valve was discharging through the vent system which is connected to the plant (customer) flare. The relief valve was stuck in the open position, so the technician then isolated and closed psv 200. After reviewing data trends, it was determined the relief valve had opened and did not reseat. The estimated time frame that the relief valve was discharging is approximately 4 hours. The estimated volume that was released is approx. 770 bbls. The relief valve was replaced on may 22, 2015. The relief valve that malfunctioned is being sent to the vendor for a failure analysis. Vendor analysis on 6/17/2015 concluded that there was a piece of welding slag between the disc and nozzle seat. This would account for the valve failing to reseat. The source of the welding slag is unknown.
Report Received Date 2015-06-17 00:00:00
Iyear 2015
Report Number 20150223
Supplemental Number 20552
Report Type Supplemental Final
Operator Id 31130 PHMSA Enforcement
Name Dcp Midstream
Operator Street Address 2331 Citywest Blvd. Hq-08-S812-02
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77042
Local Datetime 2015-05-20 18:31:00
Location Latitude 28.40632 Google Maps OpenStreetMap
Location Longitude -98.13716 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 770
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2015-05-20 18:31:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Psv In Question Was Isolated And Replaced.
On Site Datetime 2015-05-20 19:30:00
Nrc Rpt Datetime 2015-05-20 22:45:00
Nrc Rpt Num 1117141 NRC Report How to search
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Three Rivers Meter Station
Segment Name Sahi-1-4
Onshore State Abbreviation Tx
Onshore Postal Code 78022
Onshore City Name George West
Onshore County Name Live Oak
Designated Location Milepost/valve Station
Designated Name Three Rivers
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Relief Valve
Installation Year 2013
Material Involved Carbon Steel
Release Type Other
Release Type Details Psv Failed To Reseat.
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 30000
Est Cost Prop Damage 2000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 32000
Accident Psig 1350
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The scada system and controller acted correctly in the situation.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Relief Valve Ind Yes
Additional Defect Ind Yes
Additional Installation Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Piece Of Welding Slag Found In Between The Seats
Preparer Name T**** S******
Preparer Title Pipeline Compliance Specialist
Preparer Email T*******@d***********.com
Preparer Telephone 713-268-7447
Prepared Date 2015-06-25 00:00:00
Authorizer Name B****** P*****
Authorizer Telephone 713-268-7400
Authorizer Title Director Liquid Pipeline Compliance
Authorizer Email B*******@d***********.com
Narrative On may 20, 2015 at approximately 6:30 pm, dcp was delivering to a customer who had operational issues and backed up pressure to dcp's three rivers meter skid. The shutdown valve esd 100 went closed at its set point for opp of 1350 psig. An ngl technician responded on site at approximately 7:30 pm and diverted flow to an alternate customer. Another ngl technician was called to the site for assistance and arrived at approximately 9:00 pm. When the two technicians were ready to leave at 10:10 pm, they noticed the downstream side of a relief valve was iced over. The relief valve was discharging through the vent system which is connected to the plant (customer) flare. The relief valve was stuck in the open position, so the technician then isolated and closed psv 200. After reviewing data trends, it was determined the relief valve had opened and did not reseat. The estimated time frame that the relief valve was discharging is approximately 4 hours. The estimated volume that was released is approx. 770 bbls. The relief valve was replaced on may 22, 2015. The relief valve that malfunctioned is being sent to the vendor for a failure analysis. Vendor analysis on 6/17/2015 concluded that there was a piece of welding slag between the disc and nozzle seat. This would account for the valve failing to reseat. The source of the welding slag is unknown.

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