HL incident on 2015-05-04 — AZ

Operator
Navajo Nation Oil And Gas Company
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2015-05-04 12:30
Report number
Location
AZ
Narrative
The scada system shutdown the pipeline due to a leak alarm and controller notified operations manager. Operations manager directed the pipeline operator to perform visual right of way inspection and leave the pipeline shutdown. Local stakeholders notified navajo nation public safety by calling 911 due to oil leak at morgan lake station. Navajo nation public safety notified montezuma creek station and its controllers. Pipeline operator confirmed leak at morgan lake station and initiated company emergency response procedures. Pipeline operator isolated source of leak and begun containment of oil using berms and dikes. Clean up and soil contamination removal initiated immediately. Contaminated soil removed to an approved disposal facility and clean back fill material brought on location. Cleanup according to navajo nation environmental protection agency standards adhered to. Soil sampling performed by soil scientist.
Detailed record list
Report Received Date
2015-06-04 00:00:00
Iyear
2015
Report Number
20150206
Supplemental Number
20490
Report Type
Original Final
Operator Id
Name
Navajo Nation Oil And Gas Company
Operator Street Address
50 Narbono Circle West
Operator City Name
St. Michaels
Operator State Abbreviation
AZ
Operator Postal Code
86511
Local Datetime
2015-05-04 11:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
100
Recovered Bbls
100
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2015-05-04 12:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-05-04 11:30:00
Restart Datetime
2015-05-05 16:55:00
On Site Datetime
2015-05-04 13:30:00
Nrc Rpt Datetime
2015-05-04 13:10:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Morgan Lake Station
Segment Name
Running Horse Pipeline
Onshore State Abbreviation
Nm
Onshore Postal Code
87416
Onshore City Name
Not Within A Municipality
Onshore County Name
San Juan
Designated Location
Milepost/valve Station
Designated Name
Pump Station
Federal
Yes
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
2015
Material Involved
Material Other Than Carbon Steel
Material Details
Paper Gasket
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
1000
Est Cost Gas Released
6000
Est Cost Prop Damage
500
Est Cost Emergency
12000
Est Cost Environmental
36000
Est Cost Other
0
Prpty
55500
Accident Psig
280
Mop Psig
460
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
30
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Defect Ind
Yes
Preparer Name
T*** W*****
Preparer Title
Pipeline Engineer
Preparer Email
T******@n****.com
Preparer Telephone
5054090019
Preparer Fax
5055996060
Prepared Date
2015-06-04 00:00:00
Authorizer Name
T*** W*****
Authorizer Telephone
5054090019
Authorizer Title
Pipeline Engineer
Authorizer Email
T******@n****.com
Narrative
The scada system shutdown the pipeline due to a leak alarm and controller notified operations manager. Operations manager directed the pipeline operator to perform visual right of way inspection and leave the pipeline shutdown. Local stakeholders notified navajo nation public safety by calling 911 due to oil leak at morgan lake station. Navajo nation public safety notified montezuma creek station and its controllers. Pipeline operator confirmed leak at morgan lake station and initiated company emergency response procedures. Pipeline operator isolated source of leak and begun containment of oil using berms and dikes. Clean up and soil contamination removal initiated immediately. Contaminated soil removed to an approved disposal facility and clean back fill material brought on location. Cleanup according to navajo nation environmental protection agency standards adhered to. Soil sampling performed by soil scientist.
Report Received Date 2015-06-04 00:00:00
Iyear 2015
Report Number 20150206
Supplemental Number 20490
Report Type Original Final
Operator Id 31663 PHMSA Enforcement
Name Navajo Nation Oil And Gas Company
Operator Street Address 50 Narbono Circle West
Operator City Name St. Michaels
Operator State Abbreviation AZ
Operator Postal Code 86511
Local Datetime 2015-05-04 11:30:00
Location Latitude 36.715463 Google Maps OpenStreetMap
Location Longitude -108.496528 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 100
Recovered Bbls 100
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2015-05-04 12:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-05-04 11:30:00
Restart Datetime 2015-05-05 16:55:00
On Site Datetime 2015-05-04 13:30:00
Nrc Rpt Datetime 2015-05-04 13:10:00
Nrc Rpt Num 1115462 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Morgan Lake Station
Segment Name Running Horse Pipeline
Onshore State Abbreviation Nm
Onshore Postal Code 87416
Onshore City Name Not Within A Municipality
Onshore County Name San Juan
Designated Location Milepost/valve Station
Designated Name Pump Station
Federal Yes
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 2015
Material Involved Material Other Than Carbon Steel
Material Details Paper Gasket
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 1000
Est Cost Gas Released 6000
Est Cost Prop Damage 500
Est Cost Emergency 12000
Est Cost Environmental 36000
Est Cost Other 0
Prpty 55500
Accident Psig 280
Mop Psig 460
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 30
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Defect Ind Yes
Preparer Name T*** W*****
Preparer Title Pipeline Engineer
Preparer Email T******@n****.com
Preparer Telephone 5054090019
Preparer Fax 5055996060
Prepared Date 2015-06-04 00:00:00
Authorizer Name T*** W*****
Authorizer Telephone 5054090019
Authorizer Title Pipeline Engineer
Authorizer Email T******@n****.com
Narrative The scada system shutdown the pipeline due to a leak alarm and controller notified operations manager. Operations manager directed the pipeline operator to perform visual right of way inspection and leave the pipeline shutdown. Local stakeholders notified navajo nation public safety by calling 911 due to oil leak at morgan lake station. Navajo nation public safety notified montezuma creek station and its controllers. Pipeline operator confirmed leak at morgan lake station and initiated company emergency response procedures. Pipeline operator isolated source of leak and begun containment of oil using berms and dikes. Clean up and soil contamination removal initiated immediately. Contaminated soil removed to an approved disposal facility and clean back fill material brought on location. Cleanup according to navajo nation environmental protection agency standards adhered to. Soil sampling performed by soil scientist.

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