HL incident on 2015-05-09 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$11,300
Incident datetime
2015-05-09 14:00
Report number
Location
TX
Narrative
At approximately 14:00 on 5-9-15 operating personnel were making a round when a pinhole was noticed at the 6 o'clock position on the 8" bypass for ms 7. The transfer was shut down and a clamp was installed to stop the leak. The area was cleaned up and the transfer resumed.
Detailed record list
Report Received Date
2015-06-04 00:00:00
Iyear
2015
Report Number
20150202
Supplemental Number
20485
Report Type
Original Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-05-09 14:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.2
Recovered Bbls
0.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-05-09 14:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-05-09 14:00:00
Restart Datetime
2015-05-09 15:50:00
On Site Datetime
2015-05-09 14:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Ehsc
Segment Name
Manifold 100 Bypass
Onshore State Abbreviation
Tx
Onshore Postal Code
77015
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Hsc
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Pipe Wall Thickness
0.375
Pipe Smys
24000
Pipe Specification
Unknown
Pipe Seam Type
Other
Pipe Seam Details
Unknown
Pipe Manufacturer
Unknown
Pipe Coating Type
Paint
Installation Year
2001
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
30
Est Cost Prop Damage
11300
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
11330
Accident Psig
125
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control room and controller were not a contributing factor.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Not Cut Open
Int Water Acid Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
C**** A******
Preparer Title
Pipeline Compliance Specialist
Preparer Email
C*******@e****.com
Preparer Telephone
713-381-6426
Prepared Date
2015-06-04 00:00:00
Authorizer Name
C**** A******
Authorizer Telephone
713-381-6426
Authorizer Title
P
Authorizer Email
C*******@e****.com
Narrative
At approximately 14:00 on 5-9-15 operating personnel were making a round when a pinhole was noticed at the 6 o'clock position on the 8" bypass for ms 7. The transfer was shut down and a clamp was installed to stop the leak. The area was cleaned up and the transfer resumed.
Report Received Date 2015-06-04 00:00:00
Iyear 2015
Report Number 20150202
Supplemental Number 20485
Report Type Original Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-05-09 14:00:00
Location Latitude 29.74799 Google Maps OpenStreetMap
Location Longitude -95.12934 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.2
Recovered Bbls 0.2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-05-09 14:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-05-09 14:00:00
Restart Datetime 2015-05-09 15:50:00
On Site Datetime 2015-05-09 14:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Ehsc
Segment Name Manifold 100 Bypass
Onshore State Abbreviation Tx
Onshore Postal Code 77015
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Hsc
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Pipe Wall Thickness 0.375
Pipe Smys 24000
Pipe Specification Unknown
Pipe Seam Type Other
Pipe Seam Details Unknown
Pipe Manufacturer Unknown
Pipe Coating Type Paint
Installation Year 2001
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 30
Est Cost Prop Damage 11300
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 11330
Accident Psig 125
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Control room and controller were not a contributing factor.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Not Cut Open
Int Water Acid Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name C**** A******
Preparer Title Pipeline Compliance Specialist
Preparer Email C*******@e****.com
Preparer Telephone 713-381-6426
Prepared Date 2015-06-04 00:00:00
Authorizer Name C**** A******
Authorizer Telephone 713-381-6426
Authorizer Title P
Authorizer Email C*******@e****.com
Narrative At approximately 14:00 on 5-9-15 operating personnel were making a round when a pinhole was noticed at the 6 o'clock position on the 8" bypass for ms 7. The transfer was shut down and a clamp was installed to stop the leak. The area was cleaned up and the transfer resumed.

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