HL incident on 2015-04-29 — PA

Operator
Buckeye Partners, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2015-04-29 11:35
Report number
Location
PA
Narrative
While conducting a valve inspection and valve maintenance of the north platte river block valve , we experienced a packing failure while attempting to re-pack valve stem. The pipeline was shut down and valve secured. Osro was notified and is headed to site. The estimated release was 10 gallons of gasoline update: there was no soil removed. We believe the original estimate was high. No soil was removed from the sight as all spray residue had evaporated by the time the relief crew got onsite. The osro did dig up a couple spots and monitor soil for lel with no readings. Since the product was gas, no gravel was stained due to evaporation as well.
Detailed record list
Report Received Date
2015-05-28 00:00:00
Iyear
2015
Report Number
20150195
Supplemental Number
21173
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2015-04-29 11:35:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.24
Recovered Bbls
0.24
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-04-29 11:35:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-04-29 11:40:00
Restart Datetime
2015-04-29 20:14:00
On Site Datetime
2015-04-29 11:35:00
Nrc Rpt Datetime
2015-04-29 14:22:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
North Platte River Block Valve
Segment Name
Ug761nb
Onshore State Abbreviation
Mo
Onshore Postal Code
64436
Onshore City Name
Cosby
Onshore County Name
Andrew
Designated Location
Milepost/valve Station
Designated Name
Block Valbe
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Wkm
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
30
Est Cost Prop Damage
0
Est Cost Emergency
5000
Est Cost Environmental
1000
Est Cost Other
0
Prpty
6030
Accident Psig
720
Mop Psig
1393
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
278157
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak happen while maintenance was being done on the valve.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
2
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Operation Type
Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Related Failure Follow Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
M***** E*****
Preparer Title
Senior District Compliance Specialist
Preparer Email
M******@b******.com
Preparer Telephone
2192018350
Prepared Date
2016-02-26 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
6109044113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
While conducting a valve inspection and valve maintenance of the north platte river block valve , we experienced a packing failure while attempting to re-pack valve stem. The pipeline was shut down and valve secured. Osro was notified and is headed to site. The estimated release was 10 gallons of gasoline update: there was no soil removed. We believe the original estimate was high. No soil was removed from the sight as all spray residue had evaporated by the time the relief crew got onsite. The osro did dig up a couple spots and monitor soil for lel with no readings. Since the product was gas, no gravel was stained due to evaporation as well.
Report Received Date 2015-05-28 00:00:00
Iyear 2015
Report Number 20150195
Supplemental Number 21173
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2015-04-29 11:35:00
Location Latitude 39.86216 Google Maps OpenStreetMap
Location Longitude -94.695103 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.24
Recovered Bbls 0.24
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-04-29 11:35:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-04-29 11:40:00
Restart Datetime 2015-04-29 20:14:00
On Site Datetime 2015-04-29 11:35:00
Nrc Rpt Datetime 2015-04-29 14:22:00
Nrc Rpt Num 1115042 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name North Platte River Block Valve
Segment Name Ug761nb
Onshore State Abbreviation Mo
Onshore Postal Code 64436
Onshore City Name Cosby
Onshore County Name Andrew
Designated Location Milepost/valve Station
Designated Name Block Valbe
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Wkm
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 30
Est Cost Prop Damage 0
Est Cost Emergency 5000
Est Cost Environmental 1000
Est Cost Other 0
Prpty 6030
Accident Psig 720
Mop Psig 1393
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 278157
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak happen while maintenance was being done on the valve.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 2
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Operation Type Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Related Failure Follow Ind Yes
Category Type Other Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name M***** E*****
Preparer Title Senior District Compliance Specialist
Preparer Email M******@b******.com
Preparer Telephone 2192018350
Prepared Date 2016-02-26 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 6109044113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative While conducting a valve inspection and valve maintenance of the north platte river block valve , we experienced a packing failure while attempting to re-pack valve stem. The pipeline was shut down and valve secured. Osro was notified and is headed to site. The estimated release was 10 gallons of gasoline update: there was no soil removed. We believe the original estimate was high. No soil was removed from the sight as all spray residue had evaporated by the time the relief crew got onsite. The osro did dig up a couple spots and monitor soil for lel with no readings. Since the product was gas, no gravel was stained due to evaporation as well.

All rights reserved. Copyright © by ClearPHMSA