HL incident on 2015-04-29 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2015-04-29 09:00
Report number
Location
OK
Narrative
A gasket on a can pump failed after being overhauled by vendor, resulting in the release. Product was confined to the pump containment pit and recovered with a vacuum truck already on site. The correct gasket was installed and the pump was placed back in service.
Detailed record list
Report Received Date
2015-05-21 00:00:00
Iyear
2015
Report Number
20150189
Supplemental Number
20982
Report Type
Supplemental Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2015-04-29 09:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.1
Recovered Bbls
0.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-04-29 09:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Release Didn't Impact Other Facility Operations Which Remained Operating
On Site Datetime
2015-04-29 09:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Glenpool East Station
Segment Name
Station #581
Onshore State Abbreviation
Ok
Onshore Postal Code
74033
Onshore City Name
Glenpool
Onshore County Name
Tulsa
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
2015
Material Involved
Material Other Than Carbon Steel
Material Details
Gasket Material
Release Type
Leak
Leak Type
Other
Leak Type Other
Gasket
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
500
Est Cost Environmental
0
Est Cost Other
4500
Est Cost Other Details
Cost Of Utilizing Third Party Contractor's Equipment & Personnel
Prpty
5000
Accident Psig
7
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This release was the result of a mechanical failure of a gasket on a facility booster pump. Scada monitors only on/off status of booster pumps. Also this release was below system detection tolerances of cpm. No indication of an event was received in operations control. For these reasons it was determined that operations control neither caused nor contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Wrong Equipment Specified Or Installed
Operation Type
Wrong Equipment Specified Or Installed
Related Other Ind
Yes
Operation Related Details
Incorrect Gasket Supplied From Vendor
Category Type
Other Maintenance
Operator Qualification Ind
No
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7377
Prepared Date
2015-12-14 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
A gasket on a can pump failed after being overhauled by vendor, resulting in the release. Product was confined to the pump containment pit and recovered with a vacuum truck already on site. The correct gasket was installed and the pump was placed back in service.
Report Received Date 2015-05-21 00:00:00
Iyear 2015
Report Number 20150189
Supplemental Number 20982
Report Type Supplemental Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2015-04-29 09:00:00
Location Latitude 35.97974 Google Maps OpenStreetMap
Location Longitude -96.00985 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.1
Recovered Bbls 0.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-04-29 09:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Release Didn't Impact Other Facility Operations Which Remained Operating
On Site Datetime 2015-04-29 09:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Glenpool East Station
Segment Name Station #581
Onshore State Abbreviation Ok
Onshore Postal Code 74033
Onshore City Name Glenpool
Onshore County Name Tulsa
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 2015
Material Involved Material Other Than Carbon Steel
Material Details Gasket Material
Release Type Leak
Leak Type Other
Leak Type Other Gasket
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 500
Est Cost Environmental 0
Est Cost Other 4500
Est Cost Other Details Cost Of Utilizing Third Party Contractor's Equipment & Personnel
Prpty 5000
Accident Psig 7
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This release was the result of a mechanical failure of a gasket on a facility booster pump. Scada monitors only on/off status of booster pumps. Also this release was below system detection tolerances of cpm. No indication of an event was received in operations control. For these reasons it was determined that operations control neither caused nor contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Wrong Equipment Specified Or Installed
Operation Type Wrong Equipment Specified Or Installed
Related Other Ind Yes
Operation Related Details Incorrect Gasket Supplied From Vendor
Category Type Other Maintenance
Operator Qualification Ind No
Preparer Name K****** L* L*******
Preparer Title Sr. Compliance Coordinator
Preparer Email K***********@m*********.com
Preparer Telephone 918-574-7315
Preparer Fax 918-574-7377
Prepared Date 2015-12-14 00:00:00
Authorizer Name K****** L* L*******
Authorizer Telephone 918-574-7315
Authorizer Title Sr. Compliance Coordinator
Authorizer Email K***********@m*********.com
Narrative A gasket on a can pump failed after being overhauled by vendor, resulting in the release. Product was confined to the pump containment pit and recovered with a vacuum truck already on site. The correct gasket was installed and the pump was placed back in service.

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