HL incident on 2015-04-25 — TX

Operator
Enbridge Storage (Cushing) L.l.c.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000
Incident datetime
2015-04-25 21:47
Report number
Location
TX
Narrative
On april 25 at 9:47 pm cst, a maintenance technician discovered a leak on valve b227 at manifold 211. It was determined that the valve was leaking out of the stem seal packing, which resulted in the release of approximately 10 gallons of crude oil. The line was sectionalized while valve stem seal was repacked. It was determined that the cause was due to normal wear and tear. Monitoring of the valve b227 at manifold 211 is ongoing until the new valve stem is replaced which is expected to be completed by end of q2. Clean-up was completed later that night and contaminated soil was removed and disposed of at the designated disposal facility.
Detailed record list
Report Received Date
2015-05-18 00:00:00
Iyear
2015
Report Number
20150182
Supplemental Number
20455
Report Type
Original Final
Operator Id
Name
Enbridge Storage (Cushing) L.l.c.
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2015-04-25 21:47:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.24
Recovered Bbls
0.24
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-04-25 21:47:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Sectionalized While Valve Stem Was Repacked
On Site Datetime
2015-04-25 21:47:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Cushing Central Terminal
Segment Name
Manifold 211
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Payne
Designated Location
Milepost/valve Station
Designated Name
Cg
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2012
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
15
Est Cost Prop Damage
1000
Est Cost Emergency
3200
Est Cost Environmental
2000
Est Cost Other
0
Prpty
6215
Accident Psig
30
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Lack of control center involvement
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Stem Seal
Eq Additional Other Ind
Yes
Eq Additional Other Details
Normal Wear And Tear
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
2184645754
Preparer Fax
2184645992
Prepared Date
2015-05-18 00:00:00
Authorizer Name
R** C*******
Authorizer Telephone
2184645743
Authorizer Title
Manager Us Pipeline Compliance
Authorizer Email
R***********@e*******.com
Narrative
On april 25 at 9:47 pm cst, a maintenance technician discovered a leak on valve b227 at manifold 211. It was determined that the valve was leaking out of the stem seal packing, which resulted in the release of approximately 10 gallons of crude oil. The line was sectionalized while valve stem seal was repacked. It was determined that the cause was due to normal wear and tear. Monitoring of the valve b227 at manifold 211 is ongoing until the new valve stem is replaced which is expected to be completed by end of q2. Clean-up was completed later that night and contaminated soil was removed and disposed of at the designated disposal facility.
Report Received Date 2015-05-18 00:00:00
Iyear 2015
Report Number 20150182
Supplemental Number 20455
Report Type Original Final
Operator Id 39145 PHMSA Enforcement
Name Enbridge Storage (Cushing) L.l.c.
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2015-04-25 21:47:00
Location Latitude 35.945098 Google Maps OpenStreetMap
Location Longitude -96.760237 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.24
Recovered Bbls 0.24
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-04-25 21:47:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Line Was Sectionalized While Valve Stem Was Repacked
On Site Datetime 2015-04-25 21:47:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Cushing Central Terminal
Segment Name Manifold 211
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Payne
Designated Location Milepost/valve Station
Designated Name Cg
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2012
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 15
Est Cost Prop Damage 1000
Est Cost Emergency 3200
Est Cost Environmental 2000
Est Cost Other 0
Prpty 6215
Accident Psig 30
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Lack of control center involvement
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Stem Seal
Eq Additional Other Ind Yes
Eq Additional Other Details Normal Wear And Tear
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 2184645754
Preparer Fax 2184645992
Prepared Date 2015-05-18 00:00:00
Authorizer Name R** C*******
Authorizer Telephone 2184645743
Authorizer Title Manager Us Pipeline Compliance
Authorizer Email R***********@e*******.com
Narrative On april 25 at 9:47 pm cst, a maintenance technician discovered a leak on valve b227 at manifold 211. It was determined that the valve was leaking out of the stem seal packing, which resulted in the release of approximately 10 gallons of crude oil. The line was sectionalized while valve stem seal was repacked. It was determined that the cause was due to normal wear and tear. Monitoring of the valve b227 at manifold 211 is ongoing until the new valve stem is replaced which is expected to be completed by end of q2. Clean-up was completed later that night and contaminated soil was removed and disposed of at the designated disposal facility.

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