HL incident on 2015-04-17 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$83,000
Incident datetime
2015-04-17 06:48
Report number
Location
TX
Narrative
Enterprise operations supervisor was notified of a hydrocarbon leak at the mermentau pig trap site (mp 53.24) on the 12 inch lou-tex ngl pipeline in mermentau, louisiana. Enterprise houston operations control center was notified immediately to shut-in the upstream pipeline mov at castle cove valve site (hwy. 92) (mp 55.39). Downstream pump station at section 28 pulled the line pressure down to 200 psi and hcc shut-in the mov at clint road valve site (mp 34.36). A nitrogen pump truck was contracted to displace the hydrocarbons from the hwy 92 valve site across the mermentau site continuing on to the clint rd. Site. The mermentau trap isolation valves were closed as soon as the hydrocarbon release was stopped by the nitrogen displacement. No injuries reported, la. State police notifications were made, incident # 15-01484 based on the results of testing and analysis, it is concluded both the pipe nipple and bourdon tube failed to fatigue cracking which may have been produced by mechanical movements of the pig catcher, pressure pulsations within the pig catcher, or a combination of the two. Note: a second nrc number is associated with this report - # 1113985, updated volume was reported on 4/18/15 at 9:56 am. Note: time line of accident added to report on july 18, 2016 - part a4 6:48 am was time the release was determined to meet accident reporting criteria based upon the volume released exceeding 5 gallons. The accident was not immediately reportable to the nrc until 9:15 am when the determination was made that the accident would result in repairs exceeding $50,000.
Detailed record list
Report Received Date
2015-05-15 00:00:00
Iyear
2015
Report Number
20150180
Supplemental Number
21536
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-04-17 06:48:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Y-Grade
Unintentional Release Bbls
2535
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2015-04-17 06:48:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-04-17 06:48:00
Restart Datetime
2015-04-18 13:30:00
On Site Datetime
2015-04-17 06:50:00
Nrc Rpt Datetime
2015-04-17 10:06:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Automatic
Num Pub Evacuated
37
Pipe Fac Name
Lou Tex Ngl 12"
Segment Name
24740
Onshore State Abbreviation
La
Onshore Postal Code
70559
Onshore City Name
Not Within A Municipality
Onshore County Name
Acadia Parish
Designated Location
Milepost/valve Station
Designated Name
Mp 53.24
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Pipe Nipple Failure
Installation Year
2001
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
55000
Est Cost Prop Damage
83000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
32000
Est Cost Other Details
Stress Engineering Analysis.
Prpty
170000
Accident Psig
740
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
73920
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
Yes
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
A Pipe Nipple And Bourdon Tube Failed To Fatigue Cracking.
Additional Vibration Ind
Yes
Preparer Name
N***** L* G*** J**
Preparer Title
Senior Pipeline Compliance Specialist
Preparer Email
N****@e****.com
Preparer Telephone
9854934629
Prepared Date
2016-07-18 00:00:00
Authorizer Name
N***** L* G*** J**
Authorizer Telephone
9854934629
Authorizer Title
Senior Pipeline Compliance Specialist
Authorizer Email
N****@e****.com
Narrative
Enterprise operations supervisor was notified of a hydrocarbon leak at the mermentau pig trap site (mp 53.24) on the 12 inch lou-tex ngl pipeline in mermentau, louisiana. Enterprise houston operations control center was notified immediately to shut-in the upstream pipeline mov at castle cove valve site (hwy. 92) (mp 55.39). Downstream pump station at section 28 pulled the line pressure down to 200 psi and hcc shut-in the mov at clint road valve site (mp 34.36). A nitrogen pump truck was contracted to displace the hydrocarbons from the hwy 92 valve site across the mermentau site continuing on to the clint rd. Site. The mermentau trap isolation valves were closed as soon as the hydrocarbon release was stopped by the nitrogen displacement. No injuries reported, la. State police notifications were made, incident # 15-01484 based on the results of testing and analysis, it is concluded both the pipe nipple and bourdon tube failed to fatigue cracking which may have been produced by mechanical movements of the pig catcher, pressure pulsations within the pig catcher, or a combination of the two. Note: a second nrc number is associated with this report - # 1113985, updated volume was reported on 4/18/15 at 9:56 am. Note: time line of accident added to report on july 18, 2016 - part a4 6:48 am was time the release was determined to meet accident reporting criteria based upon the volume released exceeding 5 gallons. The accident was not immediately reportable to the nrc until 9:15 am when the determination was made that the accident would result in repairs exceeding $50,000.
Report Received Date 2015-05-15 00:00:00
Iyear 2015
Report Number 20150180
Supplemental Number 21536
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-04-17 06:48:00
Location Latitude 30.16 Google Maps OpenStreetMap
Location Longitude -92.55346 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Y-Grade
Unintentional Release Bbls 2535
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2015-04-17 06:48:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-04-17 06:48:00
Restart Datetime 2015-04-18 13:30:00
On Site Datetime 2015-04-17 06:50:00
Nrc Rpt Datetime 2015-04-17 10:06:00
Nrc Rpt Num 1113874 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Automatic
Num Pub Evacuated 37
Pipe Fac Name Lou Tex Ngl 12"
Segment Name 24740
Onshore State Abbreviation La
Onshore Postal Code 70559
Onshore City Name Not Within A Municipality
Onshore County Name Acadia Parish
Designated Location Milepost/valve Station
Designated Name Mp 53.24
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Pipe Nipple Failure
Installation Year 2001
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 55000
Est Cost Prop Damage 83000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 32000
Est Cost Other Details Stress Engineering Analysis.
Prpty 170000
Accident Psig 740
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 73920
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind Yes
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details A Pipe Nipple And Bourdon Tube Failed To Fatigue Cracking.
Additional Vibration Ind Yes
Preparer Name N***** L* G*** J**
Preparer Title Senior Pipeline Compliance Specialist
Preparer Email N****@e****.com
Preparer Telephone 9854934629
Prepared Date 2016-07-18 00:00:00
Authorizer Name N***** L* G*** J**
Authorizer Telephone 9854934629
Authorizer Title Senior Pipeline Compliance Specialist
Authorizer Email N****@e****.com
Narrative Enterprise operations supervisor was notified of a hydrocarbon leak at the mermentau pig trap site (mp 53.24) on the 12 inch lou-tex ngl pipeline in mermentau, louisiana. Enterprise houston operations control center was notified immediately to shut-in the upstream pipeline mov at castle cove valve site (hwy. 92) (mp 55.39). Downstream pump station at section 28 pulled the line pressure down to 200 psi and hcc shut-in the mov at clint road valve site (mp 34.36). A nitrogen pump truck was contracted to displace the hydrocarbons from the hwy 92 valve site across the mermentau site continuing on to the clint rd. Site. The mermentau trap isolation valves were closed as soon as the hydrocarbon release was stopped by the nitrogen displacement. No injuries reported, la. State police notifications were made, incident # 15-01484 based on the results of testing and analysis, it is concluded both the pipe nipple and bourdon tube failed to fatigue cracking which may have been produced by mechanical movements of the pig catcher, pressure pulsations within the pig catcher, or a combination of the two. Note: a second nrc number is associated with this report - # 1113985, updated volume was reported on 4/18/15 at 9:56 am. Note: time line of accident added to report on july 18, 2016 - part a4 6:48 am was time the release was determined to meet accident reporting criteria based upon the volume released exceeding 5 gallons. The accident was not immediately reportable to the nrc until 9:15 am when the determination was made that the accident would result in repairs exceeding $50,000.

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