HL incident on 2015-04-16 — TX

Operator
Enterprise Products Operating Llc
Cause
Incorrect Operation
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2015-04-16 07:45
Report number
Location
TX
Narrative
On april 16, 2015 ' operations personnel and contract crew had blown down launching barrel on lid 914b-100 in order to load a cleaning pig. In order to purge the launching barrel with nitrogen of hazardous vapors and not to over pressure the barrel, a pressure relief valve set at 1000 psi was installed on the launching barrel. After the launching barrel was blown down and cleaning pig inserted, the maintenance crew started to re-pressure the launching barrel with product off of the line that was flowing and operating at around 1100 psi. When the pressure on the launching barrel exceeded 1000 psi, the relief valve started relieving to the atmosphere. The valve used to pressure the launching barrel was closed and the relief valve closed off. The 1000 psig relief valve should have been replaced by one set at 1440 psig. The accident and procedures was reviewed with all personnel involved.
Detailed record list
Report Received Date
2015-05-11 00:00:00
Iyear
2015
Report Number
20150171
Supplemental Number
20428
Report Type
Original Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2015-04-16 07:45:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Rgp
Unintentional Release Bbls
2.3
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-04-16 07:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Relief Valve On Pig Trap Closed Manually.
On Site Datetime
2015-04-16 07:45:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Morgans Point To Texas Petro Olefins #3
Segment Name
914b-100
Onshore State Abbreviation
Tx
Onshore Postal Code
77209
Onshore City Name
Not Within A Municipality
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Mp 12.98
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Relief Valve
Installation Year
2015
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Pressure Exceeded Temporary Relief Valve Pressure Setting Of 1000 Psi
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
100
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
100
Accident Psig
1100
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
15
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controllers was aware of the maintenance activities on the pipeline but was not involved in causing the relief valve to release product.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Wrong Equipment Specified Or Installed
Operation Type
Wrong Equipment Specified Or Installed
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
N*** B******
Preparer Title
Sr. Pipeline Compliance Specialist
Preparer Email
W********@e****.com
Preparer Telephone
713-381-3536
Prepared Date
2015-05-11 00:00:00
Authorizer Name
N*** B******
Authorizer Telephone
713-381-3536
Authorizer Title
Sr. Pipeline Compliance Specialist
Authorizer Email
W********@e****.com
Narrative
On april 16, 2015 ' operations personnel and contract crew had blown down launching barrel on lid 914b-100 in order to load a cleaning pig. In order to purge the launching barrel with nitrogen of hazardous vapors and not to over pressure the barrel, a pressure relief valve set at 1000 psi was installed on the launching barrel. After the launching barrel was blown down and cleaning pig inserted, the maintenance crew started to re-pressure the launching barrel with product off of the line that was flowing and operating at around 1100 psi. When the pressure on the launching barrel exceeded 1000 psi, the relief valve started relieving to the atmosphere. The valve used to pressure the launching barrel was closed and the relief valve closed off. The 1000 psig relief valve should have been replaced by one set at 1440 psig. The accident and procedures was reviewed with all personnel involved.
Report Received Date 2015-05-11 00:00:00
Iyear 2015
Report Number 20150171
Supplemental Number 20428
Report Type Original Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2015-04-16 07:45:00
Location Latitude 29.57863 Google Maps OpenStreetMap
Location Longitude -95.017273 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Rgp
Unintentional Release Bbls 2.3
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-04-16 07:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Relief Valve On Pig Trap Closed Manually.
On Site Datetime 2015-04-16 07:45:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Morgans Point To Texas Petro Olefins #3
Segment Name 914b-100
Onshore State Abbreviation Tx
Onshore Postal Code 77209
Onshore City Name Not Within A Municipality
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Mp 12.98
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Relief Valve
Installation Year 2015
Material Involved Carbon Steel
Release Type Other
Release Type Details Pressure Exceeded Temporary Relief Valve Pressure Setting Of 1000 Psi
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 100
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 100
Accident Psig 1100
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 15
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controllers was aware of the maintenance activities on the pipeline but was not involved in causing the relief valve to release product.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Wrong Equipment Specified Or Installed
Operation Type Wrong Equipment Specified Or Installed
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name N*** B******
Preparer Title Sr. Pipeline Compliance Specialist
Preparer Email W********@e****.com
Preparer Telephone 713-381-3536
Prepared Date 2015-05-11 00:00:00
Authorizer Name N*** B******
Authorizer Telephone 713-381-3536
Authorizer Title Sr. Pipeline Compliance Specialist
Authorizer Email W********@e****.com
Narrative On april 16, 2015 ' operations personnel and contract crew had blown down launching barrel on lid 914b-100 in order to load a cleaning pig. In order to purge the launching barrel with nitrogen of hazardous vapors and not to over pressure the barrel, a pressure relief valve set at 1000 psi was installed on the launching barrel. After the launching barrel was blown down and cleaning pig inserted, the maintenance crew started to re-pressure the launching barrel with product off of the line that was flowing and operating at around 1100 psi. When the pressure on the launching barrel exceeded 1000 psi, the relief valve started relieving to the atmosphere. The valve used to pressure the launching barrel was closed and the relief valve closed off. The 1000 psig relief valve should have been replaced by one set at 1440 psig. The accident and procedures was reviewed with all personnel involved.

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