HL incident on 2015-04-15 — CO

Operator
Western Refining Pipeline, Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2015-04-15 06:08
Report number
Location
CO
Narrative
Crude oil overtopped a frac tank during a pipeline fill due to operator error. Once the spill was discovered the pipeline was shutdown. The spill took place adjacent to the pipeline station. Pipeline personnel used shovels to build containment. A vacuum truck was mobilized and recovered 15 barrels of crude oil and a backhoe was used to evacuate the crude impacted soil. Approximately 620 yards of dirt was removed from the site. Eight strategic samples were taken from eight different locations in the spill area. The analytical showed the area cleaned up to nmocd and blm standards.
Detailed record list
Report Received Date
2015-05-05 00:00:00
Iyear
2015
Report Number
20150161
Supplemental Number
21024
Report Type
Supplemental Final
Operator Id
Name
Western Refining Pipeline, Llc
Operator Street Address
1515 Arapahoe St. Tower 1; Suite 1600
Operator City Name
Denver
Operator State Abbreviation
CO
Operator Postal Code
80202
Local Datetime
2015-04-15 06:08:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
50
Recovered Bbls
50
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2015-04-15 06:08:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-04-15 06:10:00
Restart Datetime
2015-05-05 11:00:00
On Site Datetime
2015-04-15 08:00:00
Nrc Rpt Datetime
2015-04-15 08:27:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Texnew Mex X (Tnmx) To T Station (Mason System)
Segment Name
Mesquite Station To T Station
Onshore State Abbreviation
Nm
Onshore Postal Code
87401
Onshore City Name
Not Within A Municipality
Onshore County Name
Eddy County
Designated Location
Milepost/valve Station
Designated Name
T Station
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Temporary Frac Tanks While Filling Tnmx
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Other
Tank Vessel Details
Over Filled Frac Tank
Installation Year
2015
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1519
Est Cost Prop Damage
0
Est Cost Emergency
15000
Est Cost Environmental
93000
Est Cost Other
0
Prpty
109519
Accident Psig
60
Mop Psig
1480
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
10560
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Line fill was a manual operation with personnel onsite.
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
1
Num Contractors Failed
0
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Inadequate Monitoring
Related Failure Follow Ind
Yes
Category Type
Commissioning
Operator Qualification Ind
No
Preparer Name
D*** R*******
Preparer Title
Regulatory Compliance Supervisor
Preparer Email
D************@w**.com
Preparer Telephone
5056328006
Preparer Fax
5056324021
Prepared Date
2016-01-04 00:00:00
Authorizer Name
D*** R*******
Authorizer Telephone
5056328006
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
D************@w**.com
Narrative
Crude oil overtopped a frac tank during a pipeline fill due to operator error. Once the spill was discovered the pipeline was shutdown. The spill took place adjacent to the pipeline station. Pipeline personnel used shovels to build containment. A vacuum truck was mobilized and recovered 15 barrels of crude oil and a backhoe was used to evacuate the crude impacted soil. Approximately 620 yards of dirt was removed from the site. Eight strategic samples were taken from eight different locations in the spill area. The analytical showed the area cleaned up to nmocd and blm standards.
Report Received Date 2015-05-05 00:00:00
Iyear 2015
Report Number 20150161
Supplemental Number 21024
Report Type Supplemental Final
Operator Id 31574 PHMSA Enforcement
Name Western Refining Pipeline, Llc
Operator Street Address 1515 Arapahoe St. Tower 1; Suite 1600
Operator City Name Denver
Operator State Abbreviation CO
Operator Postal Code 80202
Local Datetime 2015-04-15 06:08:00
Location Latitude 32.062707 Google Maps OpenStreetMap
Location Longitude -103.881937 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 50
Recovered Bbls 50
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2015-04-15 06:08:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-04-15 06:10:00
Restart Datetime 2015-05-05 11:00:00
On Site Datetime 2015-04-15 08:00:00
Nrc Rpt Datetime 2015-04-15 08:27:00
Nrc Rpt Num 1113648 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Texnew Mex X (Tnmx) To T Station (Mason System)
Segment Name Mesquite Station To T Station
Onshore State Abbreviation Nm
Onshore Postal Code 87401
Onshore City Name Not Within A Municipality
Onshore County Name Eddy County
Designated Location Milepost/valve Station
Designated Name T Station
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Other
Incident Area Details Temporary Frac Tanks While Filling Tnmx
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Other
Tank Vessel Details Over Filled Frac Tank
Installation Year 2015
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1519
Est Cost Prop Damage 0
Est Cost Emergency 15000
Est Cost Environmental 93000
Est Cost Other 0
Prpty 109519
Accident Psig 60
Mop Psig 1480
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 10560
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Line fill was a manual operation with personnel onsite.
Employee Drug Test Ind No
Contractor Drug Test Ind Yes
Num Contractors Tested 1
Num Contractors Failed 0
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Inadequate Monitoring
Related Failure Follow Ind Yes
Category Type Commissioning
Operator Qualification Ind No
Preparer Name D*** R*******
Preparer Title Regulatory Compliance Supervisor
Preparer Email D************@w**.com
Preparer Telephone 5056328006
Preparer Fax 5056324021
Prepared Date 2016-01-04 00:00:00
Authorizer Name D*** R*******
Authorizer Telephone 5056328006
Authorizer Title Regulatory Compliance Supervisor
Authorizer Email D************@w**.com
Narrative Crude oil overtopped a frac tank during a pipeline fill due to operator error. Once the spill was discovered the pipeline was shutdown. The spill took place adjacent to the pipeline station. Pipeline personnel used shovels to build containment. A vacuum truck was mobilized and recovered 15 barrels of crude oil and a backhoe was used to evacuate the crude impacted soil. Approximately 620 yards of dirt was removed from the site. Eight strategic samples were taken from eight different locations in the spill area. The analytical showed the area cleaned up to nmocd and blm standards.

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