HL incident on 2015-04-08 — TX

Operator
Shell Pipeline Co., L.p.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,500
Incident datetime
2015-04-08 15:50
Report number
Location
TX
Narrative
Tank was taken out of service to perform routine maintenance. The header piping to the tank was isolated and no thermal relief was provided. Flange gasket involved in release was replaced and temporary thermal relief was installed while maintenance was conducted. A plan to provide permenant thermal relief is underway. The permit to work did not capture the risk of thermal relief within the the ptw process. Reliability and integrity team updated the mech. I&m manual sect. 3.11 to improve isolation of equipment. Maint. And ops were trained of update.
Detailed record list
Report Received Date
2015-05-01 00:00:00
Iyear
2015
Report Number
20150158
Supplemental Number
21246
Report Type
Supplemental Final
Operator Id
Name
Shell Pipeline Co., L.p.
Operator Street Address
150 North Dairy Ashford Road Wck Bldg. A
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2015-04-08 15:50:00
Location Latitude
Location Longitude
-90.68983889
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.36
Recovered Bbls
0.36
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-04-08 15:50:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Isolated Segment Of Tank Line
On Site Datetime
2015-04-08 15:50:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Houma Station
Segment Name
Houma Station
Onshore State Abbreviation
La
Onshore Postal Code
70360
Onshore City Name
Houma
Onshore County Name
Terrebonne
Designated Location
Milepost/valve Station
Designated Name
Houma Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
1968
Material Involved
Material Other Than Carbon Steel
Material Details
Gasket
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
2500
Est Cost Emergency
2500
Est Cost Environmental
0
Est Cost Other
0
Prpty
5000
Accident Psig
150
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Segment of tank line had been isolated by local operations / maintenance. Out of service for work.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Procedure Inadequate. Updated Manual Section 3.11, Mechanical I&m. Trained Maint & Ops. Personnel.
Related Inadequate Proc Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
No
Preparer Name
R****** K*****
Preparer Title
Regulatory Specialist
Preparer Email
R*************@s****.com
Preparer Telephone
713 241 1064
Preparer Fax
713 241 8498
Prepared Date
2016-03-17 00:00:00
Authorizer Name
D****** A* P****
Authorizer Telephone
713 241 2035
Authorizer Title
Integrity And Regulatory Srvc Mngr
Authorizer Email
D************@s****.com
Narrative
Tank was taken out of service to perform routine maintenance. The header piping to the tank was isolated and no thermal relief was provided. Flange gasket involved in release was replaced and temporary thermal relief was installed while maintenance was conducted. A plan to provide permenant thermal relief is underway. The permit to work did not capture the risk of thermal relief within the the ptw process. Reliability and integrity team updated the mech. I&m manual sect. 3.11 to improve isolation of equipment. Maint. And ops were trained of update.
Report Received Date 2015-05-01 00:00:00
Iyear 2015
Report Number 20150158
Supplemental Number 21246
Report Type Supplemental Final
Operator Id 31174 PHMSA Enforcement
Name Shell Pipeline Co., L.p.
Operator Street Address 150 North Dairy Ashford Road Wck Bldg. A
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2015-04-08 15:50:00
Location Latitude 29.6218722 Google Maps OpenStreetMap
Location Longitude -90.68983889 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.36
Recovered Bbls 0.36
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-04-08 15:50:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Isolated Segment Of Tank Line
On Site Datetime 2015-04-08 15:50:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Houma Station
Segment Name Houma Station
Onshore State Abbreviation La
Onshore Postal Code 70360
Onshore City Name Houma
Onshore County Name Terrebonne
Designated Location Milepost/valve Station
Designated Name Houma Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 1968
Material Involved Material Other Than Carbon Steel
Material Details Gasket
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 2500
Est Cost Emergency 2500
Est Cost Environmental 0
Est Cost Other 0
Prpty 5000
Accident Psig 150
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Segment of tank line had been isolated by local operations / maintenance. Out of service for work.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Procedure Inadequate. Updated Manual Section 3.11, Mechanical I&m. Trained Maint & Ops. Personnel.
Related Inadequate Proc Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind No
Preparer Name R****** K*****
Preparer Title Regulatory Specialist
Preparer Email R*************@s****.com
Preparer Telephone 713 241 1064
Preparer Fax 713 241 8498
Prepared Date 2016-03-17 00:00:00
Authorizer Name D****** A* P****
Authorizer Telephone 713 241 2035
Authorizer Title Integrity And Regulatory Srvc Mngr
Authorizer Email D************@s****.com
Narrative Tank was taken out of service to perform routine maintenance. The header piping to the tank was isolated and no thermal relief was provided. Flange gasket involved in release was replaced and temporary thermal relief was installed while maintenance was conducted. A plan to provide permenant thermal relief is underway. The permit to work did not capture the risk of thermal relief within the the ptw process. Reliability and integrity team updated the mech. I&m manual sect. 3.11 to improve isolation of equipment. Maint. And ops were trained of update.

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