HL incident on 2015-04-01 — OK

Operator
Oneok Ngl Pipeline, Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,500
Incident datetime
2015-04-01 08:10
Report number
Location
OK
Narrative
At 8:10 am while making rounds through the medford facility north line 4 pump yard, oneok employee noticed the outboard seal on pump #1 began to leak. Pipeline was shut down and the pump isolated. Pipeline was shut down for approximately 20 minutes while residual product was evacuated from the pump. Oneok mechanic's replaced the outboard seal on pump #1 and the pump and the pump was put back into service. Inspection of the failed seal determined the carbon face had worn, due to normal wear, and caused the release.
Detailed record list
Report Received Date
2015-04-29 00:00:00
Iyear
2015
Report Number
20150156
Supplemental Number
20393
Report Type
Original Final
Operator Id
Name
Oneok Ngl Pipeline, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2015-04-01 08:10:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
4.4
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2015-04-01 08:10:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-04-01 08:10:00
Restart Datetime
2015-04-01 08:30:00
On Site Datetime
2015-04-01 08:10:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Oneok Medford Line #4 Pump
Segment Name
Oneok North Line #4 Index #10130
Onshore State Abbreviation
Ok
Onshore Postal Code
73759
Onshore City Name
Not Within A Municipality
Onshore County Name
Grant
Designated Location
Milepost/valve Station
Designated Name
Pump Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pump
Installation Year
2013
Material Involved
Material Other Than Carbon Steel
Material Details
Carbon Pump Seal
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
190
Est Cost Prop Damage
1500
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
1690
Accident Psig
600
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Oneok employee was onsite at the time of the release and no controller actions had taken place that would have effected the pump in question.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Other Pump Ind
Seal/packing Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
Carbon Face On Seal Was Worn Down Due To Normal Wear.
Preparer Name
N*** J****
Preparer Title
Regulatory Compliance Coordinator
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2015-04-29 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Coordinator
Authorizer Email
N*********@o****.com
Narrative
At 8:10 am while making rounds through the medford facility north line 4 pump yard, oneok employee noticed the outboard seal on pump #1 began to leak. Pipeline was shut down and the pump isolated. Pipeline was shut down for approximately 20 minutes while residual product was evacuated from the pump. Oneok mechanic's replaced the outboard seal on pump #1 and the pump and the pump was put back into service. Inspection of the failed seal determined the carbon face had worn, due to normal wear, and caused the release.
Report Received Date 2015-04-29 00:00:00
Iyear 2015
Report Number 20150156
Supplemental Number 20393
Report Type Original Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2015-04-01 08:10:00
Location Latitude 36.774347 Google Maps OpenStreetMap
Location Longitude -97.756557 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 4.4
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2015-04-01 08:10:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-04-01 08:10:00
Restart Datetime 2015-04-01 08:30:00
On Site Datetime 2015-04-01 08:10:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Oneok Medford Line #4 Pump
Segment Name Oneok North Line #4 Index #10130
Onshore State Abbreviation Ok
Onshore Postal Code 73759
Onshore City Name Not Within A Municipality
Onshore County Name Grant
Designated Location Milepost/valve Station
Designated Name Pump Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Pump
Installation Year 2013
Material Involved Material Other Than Carbon Steel
Material Details Carbon Pump Seal
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 190
Est Cost Prop Damage 1500
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 1690
Accident Psig 600
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Oneok employee was onsite at the time of the release and no controller actions had taken place that would have effected the pump in question.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Other Pump Ind Seal/packing Failure
Eq Additional Other Ind Yes
Eq Additional Other Details Carbon Face On Seal Was Worn Down Due To Normal Wear.
Preparer Name N*** J****
Preparer Title Regulatory Compliance Coordinator
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2933
Prepared Date 2015-04-29 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Regulatory Compliance Coordinator
Authorizer Email N*********@o****.com
Narrative At 8:10 am while making rounds through the medford facility north line 4 pump yard, oneok employee noticed the outboard seal on pump #1 began to leak. Pipeline was shut down and the pump isolated. Pipeline was shut down for approximately 20 minutes while residual product was evacuated from the pump. Oneok mechanic's replaced the outboard seal on pump #1 and the pump and the pump was put back into service. Inspection of the failed seal determined the carbon face had worn, due to normal wear, and caused the release.

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