GTG incident on 2015-11-28 — KY

Operator
Southern Star Central Gas Pipeline, Inc
Cause
Natural Force Damage
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$276,000
Incident datetime
2015-11-28 12:36
Report number
Location
KY
Narrative
At 12:36 on 11/28/2015 ssc measurement personnel received a call from an employee with oklahoma natural gas notifying of a low pressure at the delaware tb. While in route ssc measurement notified gas control of the low pressure notification. Ssc gas control reviewed scada and could not see the tb measurement because of a communication outage due to ice on the equipment. At 14:05 on 11/28/15 ssc gas control received a call from an employee with union pacific railroad notifying of a leaking pipeline in california creek near their railroad. At 14:08 ssc gas control notified ssc measurement who was currently in route. Ssc operations arrived onsite at approximately 14:14. It was determined the upstream regulation valve would be closed to eliminate the blowing gas. The line was blown down at 15:15 causing the gas loss of approximately 100 customers in the town of delaware. Cng tank trucks were brought in and the town was returned to pressure and all customers were relit by 8:21 on 11/29/2015.
Detailed record list
Report Received Date
2015-12-26 00:00:00
Iyear
2015
Report Number
20150153
Supplemental Number
17068
Report Type
Supplemental Final
Operator Id
Name
Southern Star Central Gas Pipeline, Inc
Operator Street Address
4700 Highway 56; Box 20010
Operator City Name
Owensboro
Operator State Abbreviation
KY
Operator Postal Code
42301
Local Datetime
2015-11-28 11:00:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2015-11-28 16:04:00
Commodity Released Type
Natural Gas
Unintentional Release
739
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-11-28 15:15:00
Restart Datetime
2015-12-23 17:16:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2015-11-28 12:36:00
On Site Datetime
2015-11-28 14:14:00
On Off Shore
Onshore
Onshore State Abbreviation
Ok
Onshore Postal Code
74027
Onshore City Name
Delaware
Onshore County Name
Nowata
Designated Location
Survey Station No.
Designated Name
100/121+42
Pipe Fac Name
Line Be-008
Segment Name
Delaware Tb
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Exposur In A Creek Bed
Crossing
Yes
Water Crossing Ind
Yes
Water Type
Uncased
Water Name
California Creek
Water Depth
Unknown
Water Subtype
Below Water, Pipe On Or Above Bottom
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
4
Pipe Wall Thickness
0.142
Pipe Smys
35000
Pipe Specification
Api
Pipe Seam Type
Longitudinal Erw - Low Frequency
Pipe Manufacturer
Newport Steel
Pipe Coating Type
Field Applied Epoxy
Installation Year
1958
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
1
Puncture Circum
11
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
30
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
1430
Est Cost Intentional Release
0
Est Cost Prop Damage
276000
Est Cost Emergency
2500
Est Cost Other
0
Prpty
279930
Accident Psig
70
Mop Psig
90
Mop Cfr Section
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
20646
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
No Pigging Facilities. Line Would Have To Be Cut To Run Tethered Tools
Operation Complications Ind
Yes
Low Op Pressure Ind
Yes
Low Flow Ind
Yes
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
No
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Public
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Heavy Rains/floods
Natural Force Type
Heavy Rains/floods
Heavy Rains Subtype
Other
Nf Other Details
Heavy Rain And Flooding Cause Large Debris/tree To Strike The 4" Ssc Pipeline That Was Exposed In The Creak Ditch.
Nf Extreme Weather Ind
No
Preparer Name
D**** C*****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
D***********@s****.com
Preparer Telephone
2708524391
Authorizer Name
D**** S*******
Authorizer Title
Pipeline Compliance Manager
Authorizer Telephone
2708524424
Authorizer Email
D***************@s****.com
Narrative
At 12:36 on 11/28/2015 ssc measurement personnel received a call from an employee with oklahoma natural gas notifying of a low pressure at the delaware tb. While in route ssc measurement notified gas control of the low pressure notification. Ssc gas control reviewed scada and could not see the tb measurement because of a communication outage due to ice on the equipment. At 14:05 on 11/28/15 ssc gas control received a call from an employee with union pacific railroad notifying of a leaking pipeline in california creek near their railroad. At 14:08 ssc gas control notified ssc measurement who was currently in route. Ssc operations arrived onsite at approximately 14:14. It was determined the upstream regulation valve would be closed to eliminate the blowing gas. The line was blown down at 15:15 causing the gas loss of approximately 100 customers in the town of delaware. Cng tank trucks were brought in and the town was returned to pressure and all customers were relit by 8:21 on 11/29/2015.
Report Received Date 2015-12-26 00:00:00
Iyear 2015
Report Number 20150153
Supplemental Number 17068
Report Type Supplemental Final
Operator Id 31711 PHMSA Enforcement
Name Southern Star Central Gas Pipeline, Inc
Operator Street Address 4700 Highway 56; Box 20010
Operator City Name Owensboro
Operator State Abbreviation KY
Operator Postal Code 42301
Local Datetime 2015-11-28 11:00:00
Location Latitude 36.75051 Google Maps OpenStreetMap
Location Longitude -95.634032 Google Maps OpenStreetMap
Nrc Rpt Num 1134450 NRC Report How to search
Nrc Rpt Datetime 2015-11-28 16:04:00
Commodity Released Type Natural Gas
Unintentional Release 739
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-11-28 15:15:00
Restart Datetime 2015-12-23 17:16:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2015-11-28 12:36:00
On Site Datetime 2015-11-28 14:14:00
On Off Shore Onshore
Onshore State Abbreviation Ok
Onshore Postal Code 74027
Onshore City Name Delaware
Onshore County Name Nowata
Designated Location Survey Station No.
Designated Name 100/121+42
Pipe Fac Name Line Be-008
Segment Name Delaware Tb
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Other
Incident Area Details Exposur In A Creek Bed
Crossing Yes
Water Crossing Ind Yes
Water Type Uncased
Water Name California Creek
Water Depth Unknown
Water Subtype Below Water, Pipe On Or Above Bottom
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 4
Pipe Wall Thickness 0.142
Pipe Smys 35000
Pipe Specification Api
Pipe Seam Type Longitudinal Erw - Low Frequency
Pipe Manufacturer Newport Steel
Pipe Coating Type Field Applied Epoxy
Installation Year 1958
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 1
Puncture Circum 11
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 30
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 1430
Est Cost Intentional Release 0
Est Cost Prop Damage 276000
Est Cost Emergency 2500
Est Cost Other 0
Prpty 279930
Accident Psig 70
Mop Psig 90
Mop Cfr Section 192.619(C) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 20646
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details No Pigging Facilities. Line Would Have To Be Cut To Run Tethered Tools
Operation Complications Ind Yes
Low Op Pressure Ind Yes
Low Flow Ind Yes
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind No
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Public
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Heavy Rains/floods
Natural Force Type Heavy Rains/floods
Heavy Rains Subtype Other
Nf Other Details Heavy Rain And Flooding Cause Large Debris/tree To Strike The 4" Ssc Pipeline That Was Exposed In The Creak Ditch.
Nf Extreme Weather Ind No
Preparer Name D**** C*****
Preparer Title Pipeline Compliance Engineer
Preparer Email D***********@s****.com
Preparer Telephone 2708524391
Authorizer Name D**** S*******
Authorizer Title Pipeline Compliance Manager
Authorizer Telephone 2708524424
Authorizer Email D***************@s****.com
Narrative At 12:36 on 11/28/2015 ssc measurement personnel received a call from an employee with oklahoma natural gas notifying of a low pressure at the delaware tb. While in route ssc measurement notified gas control of the low pressure notification. Ssc gas control reviewed scada and could not see the tb measurement because of a communication outage due to ice on the equipment. At 14:05 on 11/28/15 ssc gas control received a call from an employee with union pacific railroad notifying of a leaking pipeline in california creek near their railroad. At 14:08 ssc gas control notified ssc measurement who was currently in route. Ssc operations arrived onsite at approximately 14:14. It was determined the upstream regulation valve would be closed to eliminate the blowing gas. The line was blown down at 15:15 causing the gas loss of approximately 100 customers in the town of delaware. Cng tank trucks were brought in and the town was returned to pressure and all customers were relit by 8:21 on 11/29/2015.

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