GTG incident on 2015-11-21 — NV

Operator
Paiute Pipeline Co
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$27,452
Incident datetime
2015-11-21 15:53
Report number
Location
NV
Narrative
On november 21, 2015, the 8-inch carson lateral was punctured on the south side of mica drive at US-395 during an in-line inspection (ili) tool run. The puncture occurred at a drop section containing 45-degree elbows installed in 1987 as part of a relocation for the construction of mica drive. An investigation on the cause of the incident has been completed and it was determined that during the ili of the carson lateral, the leading eye of the mfl tool struck the inside of the 45 degree elbow and caused a puncture in the pipeline. Company employees and contractors were stationed at the segment isolation valves as part of the ili procedure allowing for a rapid response and shutdown of the pipeline as part of the isolation plan. Public and private property damage includes six vehicles and a landscape retaining wall as a result of the blowing dirt and rocks. The magnetic flux leakage ili tool was also damaged.
Detailed record list
Report Received Date
2015-12-18 00:00:00
Iyear
2015
Report Number
20150150
Supplemental Number
17146
Report Type
Supplemental Final
Operator Id
Name
Paiute Pipeline Co
Operator Street Address
5241 Spring Mountain Road
Operator City Name
Las Vegas
Operator State Abbreviation
NV
Operator Postal Code
89150
Local Datetime
2015-11-21 15:50:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2015-11-21 16:36:00
Commodity Released Type
Natural Gas
Unintentional Release
625
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-11-21 15:55:00
Restart Datetime
2015-11-25 10:27:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2015-11-21 15:53:00
On Site Datetime
2015-11-21 15:53:00
On Off Shore
Onshore
Onshore State Abbreviation
Nv
Onshore Postal Code
89705
Onshore City Name
Carson City
Onshore County Name
Douglas
Designated Location
Milepost
Designated Name
Ca-57.30
Pipe Fac Name
Carson Lateral
Segment Name
Mica Drive Relocation
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
156
Crossing
Yes
Road Crossing Ind
Yes
Road Type
Uncased
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
8
Pipe Wall Thickness
0.188
Pipe Smys
42000
Pipe Specification
Api 5l
Pipe Seam Type
Longitudinal Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Extruded Polyehylene
Installation Year
1987
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
1.4
Puncture Circum
0.6
Class Location Type
Class 3 Location
Could Be Hca
No
Pir Radius
126
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
400000
Est Cost Unintentional Release
1479
Est Cost Intentional Release
0
Est Cost Prop Damage
27452
Est Cost Emergency
962
Est Cost Other
0
Prpty
429893
Accident Psig
502
Mop Psig
520
Mop Cfr Section
192.619(A)(2)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
33370
Internal Inspection Ind
Yes
Operation Complications Ind
Yes
Low Op Pressure Ind
Yes
Low Flow Ind
Yes
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A mechanical puncture occurred during an in-line inspection (ili) of the carson lateral. The punctured line was isolated from the parallel carson loop line. The scada information was limited to the carson loop due to the pipeline configuration as part of the ili procedure.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
Yes
Num Employees Tested
5
Num Employees Failed
0
Num Contractors Tested
2
Num Contractors Failed
0
Cause
Other Outside Force Damage
Cause Details
Other Outside Force Damage
Outside Force Type
Other Outside Force Damage
Osf Other Details
Paiute Pipeline Was Running An Inline Inspection Tool Through The Carson Lateral. The Leading Eye Of The Mfl Tool Struck The Inside Of A Long Radius 45 Degree Elbow, Puncturing The Pipe And Resulting In A Rupture.
Preparer Name
K***** C******
Preparer Title
Manager Of Engineering Paiute
Preparer Email
K*************@s****.com
Preparer Telephone
775-887-2814
Preparer Fax
775-882-4346
Authorizer Name
J*** M*****
Authorizer Title
Director Of Gas Operations Paiute
Authorizer Telephone
775-887-2805
Authorizer Email
J**********@s****.com
Narrative
On november 21, 2015, the 8-inch carson lateral was punctured on the south side of mica drive at US-395 during an in-line inspection (ili) tool run. The puncture occurred at a drop section containing 45-degree elbows installed in 1987 as part of a relocation for the construction of mica drive. An investigation on the cause of the incident has been completed and it was determined that during the ili of the carson lateral, the leading eye of the mfl tool struck the inside of the 45 degree elbow and caused a puncture in the pipeline. Company employees and contractors were stationed at the segment isolation valves as part of the ili procedure allowing for a rapid response and shutdown of the pipeline as part of the isolation plan. Public and private property damage includes six vehicles and a landscape retaining wall as a result of the blowing dirt and rocks. The magnetic flux leakage ili tool was also damaged.
Report Received Date 2015-12-18 00:00:00
Iyear 2015
Report Number 20150150
Supplemental Number 17146
Report Type Supplemental Final
Operator Id 15033 PHMSA Enforcement
Name Paiute Pipeline Co
Operator Street Address 5241 Spring Mountain Road
Operator City Name Las Vegas
Operator State Abbreviation NV
Operator Postal Code 89150
Local Datetime 2015-11-21 15:50:00
Location Latitude 39.09108 Google Maps OpenStreetMap
Location Longitude -119.77467 Google Maps OpenStreetMap
Nrc Rpt Num 1134017 NRC Report How to search
Nrc Rpt Datetime 2015-11-21 16:36:00
Commodity Released Type Natural Gas
Unintentional Release 625
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-11-21 15:55:00
Restart Datetime 2015-11-25 10:27:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2015-11-21 15:53:00
On Site Datetime 2015-11-21 15:53:00
On Off Shore Onshore
Onshore State Abbreviation Nv
Onshore Postal Code 89705
Onshore City Name Carson City
Onshore County Name Douglas
Designated Location Milepost
Designated Name Ca-57.30
Pipe Fac Name Carson Lateral
Segment Name Mica Drive Relocation
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 156
Crossing Yes
Road Crossing Ind Yes
Road Type Uncased
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 8
Pipe Wall Thickness 0.188
Pipe Smys 42000
Pipe Specification Api 5l
Pipe Seam Type Longitudinal Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Extruded Polyehylene
Installation Year 1987
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 1.4
Puncture Circum 0.6
Class Location Type Class 3 Location
Could Be Hca No
Pir Radius 126
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 400000
Est Cost Unintentional Release 1479
Est Cost Intentional Release 0
Est Cost Prop Damage 27452
Est Cost Emergency 962
Est Cost Other 0
Prpty 429893
Accident Psig 502
Mop Psig 520
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 33370
Internal Inspection Ind Yes
Operation Complications Ind Yes
Low Op Pressure Ind Yes
Low Flow Ind Yes
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A mechanical puncture occurred during an in-line inspection (ili) of the carson lateral. The punctured line was isolated from the parallel carson loop line. The scada information was limited to the carson loop due to the pipeline configuration as part of the ili procedure.
Employee Drug Test Ind Yes
Contractor Drug Test Ind Yes
Num Employees Tested 5
Num Employees Failed 0
Num Contractors Tested 2
Num Contractors Failed 0
Cause Other Outside Force Damage
Cause Details Other Outside Force Damage
Outside Force Type Other Outside Force Damage
Osf Other Details Paiute Pipeline Was Running An Inline Inspection Tool Through The Carson Lateral. The Leading Eye Of The Mfl Tool Struck The Inside Of A Long Radius 45 Degree Elbow, Puncturing The Pipe And Resulting In A Rupture.
Preparer Name K***** C******
Preparer Title Manager Of Engineering Paiute
Preparer Email K*************@s****.com
Preparer Telephone 775-887-2814
Preparer Fax 775-882-4346
Authorizer Name J*** M*****
Authorizer Title Director Of Gas Operations Paiute
Authorizer Telephone 775-887-2805
Authorizer Email J**********@s****.com
Narrative On november 21, 2015, the 8-inch carson lateral was punctured on the south side of mica drive at US-395 during an in-line inspection (ili) tool run. The puncture occurred at a drop section containing 45-degree elbows installed in 1987 as part of a relocation for the construction of mica drive. An investigation on the cause of the incident has been completed and it was determined that during the ili of the carson lateral, the leading eye of the mfl tool struck the inside of the 45 degree elbow and caused a puncture in the pipeline. Company employees and contractors were stationed at the segment isolation valves as part of the ili procedure allowing for a rapid response and shutdown of the pipeline as part of the isolation plan. Public and private property damage includes six vehicles and a landscape retaining wall as a result of the blowing dirt and rocks. The magnetic flux leakage ili tool was also damaged.

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