GTG incident on 2015-11-10 — NE

Operator
Northern Natural Gas Co
Cause
Notification Issue
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2015-11-10 09:12
Report number
Location
NE
Narrative
On november 10, 2015 at approximately 08:30 the pipeline was struck and damaged by a ditch witch rt95 chain type trencher. The operator of the equipment immediately shut off the trencher, left it in place against the pipeline, and retreated to safety. There was no fire, no injuries and no casualties. No one was evacuated from their home. The operator of the trencher, jaqs irrigation and trenching, was doing subcontract work for mussman excavating. Neither contractor made the required one-call. The pipeline is a 10-inch operating at about 500 psi at the time of the incident. The line hit was the only damage. The pipeline was 42-inches deep. The trencher tooth caused a 1-inch by 2-inch puncture. The damaged section was replaced with a 10-foot length of new pipe. About 5,000 mcf of natural gas was released due to the damage and during repairs. There were no service interruptions because the company used volume bottle trailers to provide temporary service to the town of western, ne.
Detailed record list
Report Received Date
2015-12-09 00:00:00
Iyear
2015
Report Number
20150145
Supplemental Number
17064
Report Type
Supplemental
Operator Id
Name
Northern Natural Gas Co
Operator Street Address
1111 South 103rd Street
Operator City Name
Omaha
Operator State Abbreviation
NE
Operator Postal Code
68124
Local Datetime
2015-11-10 08:30:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2015-11-10 09:45:00
Commodity Released Type
Natural Gas
Unintentional Release
4000
Intentional Release
1300
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2015-11-10 13:41:00
Restart Datetime
2015-11-11 08:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2015-11-10 09:12:00
On Site Datetime
2015-11-10 10:12:00
On Off Shore
Onshore
Onshore State Abbreviation
Ne
Onshore Postal Code
38453
Onshore City Name
Not Within A Municipality
Onshore County Name
Saline
Designated Location
Milepost
Designated Name
Mp 35.53
Pipe Fac Name
Kansas-Nebraska 10-Inch
Segment Name
Neb49401
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
42
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10
Pipe Wall Thickness
0.188
Pipe Smys
42000
Pipe Specification
Api 5lx
Pipe Seam Type
Longitudinal Erw - Low Frequency
Pipe Manufacturer
Youngstown
Pipe Coating Type
Coal Tar
Installation Year
1962
Manufactured Year
1962
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
1
Puncture Circum
2
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
195
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
12000
Est Cost Intentional Release
3900
Est Cost Prop Damage
5000
Est Cost Emergency
97947
Est Cost Other
0
Prpty
118847
Accident Psig
502
Mop Psig
800
Mop Cfr Section
192.619(A)(1)
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
105600
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The third party that caused the incident immediately dialed 911. Our first notification came from them.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Landowner
Excavator Type
Contractor
Excavator Equipment
Trencher
Work Performed
Drainage
One Call Notified Ind
No
Service Interruption
No
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Preparer Name
J*** A G******
Preparer Title
Sr. Corrosion Specialist
Preparer Email
J***********@n****.com
Preparer Telephone
402-398-7494
Authorizer Name
T***** C******
Authorizer Title
Sr. Director Of Pipeline Safety And Risk
Authorizer Telephone
402-398-7715
Authorizer Email
T*************@n****.com
Narrative
On november 10, 2015 at approximately 08:30 the pipeline was struck and damaged by a ditch witch rt95 chain type trencher. The operator of the equipment immediately shut off the trencher, left it in place against the pipeline, and retreated to safety. There was no fire, no injuries and no casualties. No one was evacuated from their home. The operator of the trencher, jaqs irrigation and trenching, was doing subcontract work for mussman excavating. Neither contractor made the required one-call. The pipeline is a 10-inch operating at about 500 psi at the time of the incident. The line hit was the only damage. The pipeline was 42-inches deep. The trencher tooth caused a 1-inch by 2-inch puncture. The damaged section was replaced with a 10-foot length of new pipe. About 5,000 mcf of natural gas was released due to the damage and during repairs. There were no service interruptions because the company used volume bottle trailers to provide temporary service to the town of western, ne.
Report Received Date 2015-12-09 00:00:00
Iyear 2015
Report Number 20150145
Supplemental Number 17064
Report Type Supplemental
Operator Id 13750 PHMSA Enforcement
Name Northern Natural Gas Co
Operator Street Address 1111 South 103rd Street
Operator City Name Omaha
Operator State Abbreviation NE
Operator Postal Code 68124
Local Datetime 2015-11-10 08:30:00
Location Latitude 40.453494 Google Maps OpenStreetMap
Location Longitude -97.316222 Google Maps OpenStreetMap
Nrc Rpt Num 1133046 NRC Report How to search
Nrc Rpt Datetime 2015-11-10 09:45:00
Commodity Released Type Natural Gas
Unintentional Release 4000
Intentional Release 1300
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2015-11-10 13:41:00
Restart Datetime 2015-11-11 08:00:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2015-11-10 09:12:00
On Site Datetime 2015-11-10 10:12:00
On Off Shore Onshore
Onshore State Abbreviation Ne
Onshore Postal Code 38453
Onshore City Name Not Within A Municipality
Onshore County Name Saline
Designated Location Milepost
Designated Name Mp 35.53
Pipe Fac Name Kansas-Nebraska 10-Inch
Segment Name Neb49401
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 42
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10
Pipe Wall Thickness 0.188
Pipe Smys 42000
Pipe Specification Api 5lx
Pipe Seam Type Longitudinal Erw - Low Frequency
Pipe Manufacturer Youngstown
Pipe Coating Type Coal Tar
Installation Year 1962
Manufactured Year 1962
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 1
Puncture Circum 2
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 195
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 12000
Est Cost Intentional Release 3900
Est Cost Prop Damage 5000
Est Cost Emergency 97947
Est Cost Other 0
Prpty 118847
Accident Psig 502
Mop Psig 800
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 105600
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The third party that caused the incident immediately dialed 911. Our first notification came from them.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Landowner
Excavator Type Contractor
Excavator Equipment Trencher
Work Performed Drainage
One Call Notified Ind No
Service Interruption No
Root Cause Category Notification Issue
Root Cause Type No Notification Made To The One-Call Center/811
Preparer Name J*** A G******
Preparer Title Sr. Corrosion Specialist
Preparer Email J***********@n****.com
Preparer Telephone 402-398-7494
Authorizer Name T***** C******
Authorizer Title Sr. Director Of Pipeline Safety And Risk
Authorizer Telephone 402-398-7715
Authorizer Email T*************@n****.com
Narrative On november 10, 2015 at approximately 08:30 the pipeline was struck and damaged by a ditch witch rt95 chain type trencher. The operator of the equipment immediately shut off the trencher, left it in place against the pipeline, and retreated to safety. There was no fire, no injuries and no casualties. No one was evacuated from their home. The operator of the trencher, jaqs irrigation and trenching, was doing subcontract work for mussman excavating. Neither contractor made the required one-call. The pipeline is a 10-inch operating at about 500 psi at the time of the incident. The line hit was the only damage. The pipeline was 42-inches deep. The trencher tooth caused a 1-inch by 2-inch puncture. The damaged section was replaced with a 10-foot length of new pipe. About 5,000 mcf of natural gas was released due to the damage and during repairs. There were no service interruptions because the company used volume bottle trailers to provide temporary service to the town of western, ne.

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